一套降低油井生产含水率的解决方案

A. A. Isaev, R. Takhautdinov, V. I. Malykhin, A. A. Sharifullin
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引用次数: 1

摘要

本文介绍了一系列降低含水率的措施,并开发了一种测量含水率的技术解决方案:使用移动设备测量井产出的含水率、流速和气油比。示踪剂测试和一致性控制操作-在这些操作之后,Bashkirian阶段反应井的含水率降低了16.6%。通过水流控制、流偏和修复生产套管损坏,可以减少采出水的采出,从而降低石油生产成本。液相分离装置的开发使油和水交替输送到井下泵的进水口。
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A Set of Solutions to Reduce the Water Cut in Well Production
This paper presents a set of activities to reduce water cut and develop a technical solution to measure water cut: measurement of watercut, flow rates and gas-oil ratio of a well output using a mobile unit. tracer tests and conformance control operations - watercut of reacting wells within Bashkirian stage decreased by 16,6% after those operations were performed. water flow control, flow deviation and remedying production casing damages made it possible to reduce extraction of produced water and, accordingly, the cost of oil production. development of Liquid Phase Separation Device enabled alternate delivery of oil and water to the intake of downhole pump.
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