Ganja氧化铝厂明矾石加工工艺问题分析及解决途径

Eldar I. Taghiyev
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引用次数: 1

摘要

1965年,Ganja氧化铝厂(GAP)开始实施碱性还原技术,用于工业规模的明矾石矿石加工。技术上的缺陷,加上设计上的错误,导致生产无利可图。自该厂建立以来,通过碱性技术和硬件设计进行了研究,以消除还原过程中的缺陷。开发了一种“反向”方案,用于用KOH溶液转化硫酸钠恢复明矾石的水化学处理。尽管消除了碱还原技术的一些缺点,但某些缺点仍然存在,特别是- 1)在焙烧和回收过程中,流化床炉的窑炉产生了大量的气体和粉尘;2)明矾石粉的回收时间不足,使工艺的技术经济方面复杂化和恶化;3)氧化铝在焙烧和还原过程中的钝化;4)商品化产品中氧化铝产率低(≤75%);5)大量的固体废物——每1吨AL2O3产生5吨红污泥,以及误差。因此,明矾石矿石加工生产线于1992年停产,此后一直没有运营。本文介绍了明矾石选矿新工艺的开发和改进,即钾碱法和钠碱法。提出了采用新型碱钠工艺,以钠(碳酸钠)代替钾。第一次浸出液经硫酸钠与氯化钾转化处理后,生成硫酸钾和氯化钠。使用钠碱技术使我们能够获得与钾碱技术相同的产品,并增加了产品-食盐。流化床炉被一种新型的窑炉所取代。
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Analysis of Technological Issues, Related to Processing of Alunite at Ganja Alumina Plant (GAP), and Ways of Their Solving
In 1965, the Ganja Alumina plant (GAP) started implementing an alkaline reduction technology for processing of alunite ore on an industrial scale. Technological deficiencies, together with design errors, led to unprofitable production. Since the plant was established, studies have been conducted to eliminate deficiencies in the reduction process, through alkaline technology and hardware design. A “reversed” scheme was developed for hydrochemical processing of alunite restored with the conversion of sodium sulphates using a KOH solution. Despite the elimination of several shortcomings in alkaline reduction technology, certain drawbacks remained, in particular- 1) significant emission of gas and dust from the kilns of fluidized bed furnace during roasting and recovery; 2) insufficient time for recovery of alunite powder, which complicates and worsens the technological and economic aspects of the process; 3) passivation of alumina in the roasting and reduction processes; 4) low yield alumina yield in the commercial product (≤ 75%); and 5) a significant amount of solid waste- 5 tonnes of red sludge per 1 tonne of AL2O3, and errors. As a result, the alunite ore processing line ceased production in 1992 and has not operated since. This article is devoted to the development of new technologies and the improvement of a new potash-alkaline method and new soda-alkaline technology for processing alunite ores. The replacement of potash with soda (sodium carbonate), using new soda-alkaline technology, is proposed. Processing of solution from the first leach with sodium sulphate by conversion with KCl leads to production of K2SO4 and NaCl. Use of the soda-alkaline technology allowed us to obtain the same products as with potash-alkaline technology, with an additional product – table salt. The fluidized bed furnace was replaced by a new type of kiln.
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