Evaluation of a New Treatment to Remove Calcium Sulfate Scale: Lab Studies and Field Application.

A. Ibrahim, H. Nasr-El-Din, Mohamed Abd El-baqi, A. Abdelhay, H. Farouk, A. Aref, Ahmed Reda, M. Rafaat, M. Gamal
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引用次数: 2

Abstract

Scale deposition has been a significant problem in the oil and gas industry. Scale deposition has an adverse impact on production and injection operations. The precipitation of scale in the near-wellbore area will diminish the productivity of the production wells and loss of the injectivity of water injection wells. This paper presents a new non-corrosive agent to remove calcium carbonate, and calcium sulfate scales. Two sets of coreflood experiments were conducted to evaluate the chemical to remove anhydrite depositions. Coreflood experiments were conducted by using the new scale remover to stimulate dolomite cores with anhydrite content of 30 wt% at 250°F. Other experiments were conducted with the Bandera sandstone cores. Calcium sulfate was precipitated inside the pores and then the chemical was used to treat the cores to remove this damage. Effluent samples were collected and analyzed with ICP for sulfur and calcium concentrations. CT scan was used to detect the dissolution and the deposition of scale inside the cores. The chemical was applied on several oil wells from the Nukhul sandstone formation. Coreflood results show increasing the permeability of the dolomite core to 4 times of its initial value and ICP results show 1:1 calcium to sulfur concentrations. The second coreflood experiments showed the ability of the dissolving agent to remove the precipitated scale completely with (final permeability =initial permeability) with no effect on clays. In the field case, the treatment was conducted and placed using a coiled tubing without using additional additives such as corrosion inhibitors, intensifiers, and iron control agents. The success of this treatment was realized by increasing the well production 4 times its initial oil production per day. Field data and the lab results highlight that the de-scaling solution is an effective fluid for calcium sulfate scale.
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一种去除硫酸钙垢的新方法的评价:实验室研究和现场应用。
水垢沉积一直是油气行业的一大难题。结垢对生产和注入作业有不利影响。近井区结垢的沉淀会降低生产井的产能,降低注水井的注入能力。本文介绍了一种去除碳酸钙、硫酸钙水垢的新型无腐蚀性清洗剂。进行了两组岩心驱替实验,以评价化学药剂去除硬石膏沉积的效果。在250°F下,使用新型除垢剂对硬石膏含量为30%的白云岩岩心进行了驱油实验。其他实验是用班德拉砂岩岩心进行的。在孔隙中沉淀硫酸钙,然后用化学物质处理岩心以消除这种损害。收集废水样品,用ICP分析硫和钙浓度。CT扫描检测岩心内的溶蚀和水垢沉积情况。该化学品被应用于Nukhul砂岩地层的几口油井。岩心驱油结果表明,白云岩岩心渗透率提高到初始值的4倍,ICP结果显示钙硫比为1:1。第二次岩心驱油实验表明,溶出剂能够完全去除沉淀垢,且(最终渗透率=初始渗透率)对粘土没有影响。在现场作业中,使用连续油管进行了处理,没有使用其他添加剂,如缓蚀剂、增强剂和铁控制剂。通过将油井产量提高到初始产油量的4倍,该处理方法取得了成功。现场数据和实验室结果表明,该除垢液是一种有效的硫酸钙除垢液。
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