Transient Stability improvement using series reactors: A case study

Gd Jennings, Lnf de Villiers
{"title":"Transient Stability improvement using series reactors: A case study","authors":"Gd Jennings, Lnf de Villiers","doi":"10.1109/EPEC.2015.7379966","DOIUrl":null,"url":null,"abstract":"A solution is presented that improves the transient stability of a remotely connected 5640 MVA power station that is to be built 10km from an existing 4428 MVA power station through the use of fixed mH size air-core reactors. The main component of the solution involves dividing each 6-pack power station into two 3-pack stations by the use of series busbar reactors and also linking the two neighbouring power stations through a series reactor. The paper explains the impact these reactors have on synchronizing power flows and shows that optimal values for these reactors exist that maximize transient stability. The complete Transient Stability Scheme (TSS) has little negative impact on transmission and generation plant and increases the Critical Clearing Time (CCT) from 43ms to 88ms.","PeriodicalId":231255,"journal":{"name":"2015 IEEE Electrical Power and Energy Conference (EPEC)","volume":"70 1","pages":"0"},"PeriodicalIF":0.0000,"publicationDate":"2015-10-01","publicationTypes":"Journal Article","fieldsOfStudy":null,"isOpenAccess":false,"openAccessPdf":"","citationCount":"0","resultStr":null,"platform":"Semanticscholar","paperid":null,"PeriodicalName":"2015 IEEE Electrical Power and Energy Conference (EPEC)","FirstCategoryId":"1085","ListUrlMain":"https://doi.org/10.1109/EPEC.2015.7379966","RegionNum":0,"RegionCategory":null,"ArticlePicture":[],"TitleCN":null,"AbstractTextCN":null,"PMCID":null,"EPubDate":"","PubModel":"","JCR":"","JCRName":"","Score":null,"Total":0}
引用次数: 0

Abstract

A solution is presented that improves the transient stability of a remotely connected 5640 MVA power station that is to be built 10km from an existing 4428 MVA power station through the use of fixed mH size air-core reactors. The main component of the solution involves dividing each 6-pack power station into two 3-pack stations by the use of series busbar reactors and also linking the two neighbouring power stations through a series reactor. The paper explains the impact these reactors have on synchronizing power flows and shows that optimal values for these reactors exist that maximize transient stability. The complete Transient Stability Scheme (TSS) has little negative impact on transmission and generation plant and increases the Critical Clearing Time (CCT) from 43ms to 88ms.
查看原文
分享 分享
微信好友 朋友圈 QQ好友 复制链接
本刊更多论文
利用串联电抗器改善瞬态稳定性:一个案例研究
本文提出了一种解决方案,通过使用固定mH大小的空芯电抗器,提高距离现有4428mva电站10km远的5640mva远程连接电站的暂态稳定性。该解决方案的主要组成部分包括使用串联母线电抗器将每个6包电站分成两个3包电站,并通过串联电抗器将两个相邻的电站连接起来。本文解释了这些电抗器对同步潮流的影响,并表明存在使这些电抗器暂态稳定性最大化的最优值。完整的暂态稳定方案(TSS)对输变电和发电厂的负面影响很小,并将临界清除时间(CCT)从43ms提高到88ms。
本文章由计算机程序翻译,如有差异,请以英文原文为准。
求助全文
约1分钟内获得全文 去求助
来源期刊
自引率
0.00%
发文量
0
期刊最新文献
Comparison between numerical and analytical methods of AC resistance evaluation for Medium Frequency Transformers: Validation on a prototype Improved control strategy of full-bridge modular multilevel converter Appliance scheduling optimization in smart home networks comprising of smart appliances and a photovoltaic panel Dynamic Reactive Power Compensation for voltage support using Static VAR Compensator (SVC) In Saudi Arabia Observability analysis of power systems in the presence of hybrid measurements
×
引用
GB/T 7714-2015
复制
MLA
复制
APA
复制
导出至
BibTeX EndNote RefMan NoteFirst NoteExpress
×
×
提示
您的信息不完整,为了账户安全,请先补充。
现在去补充
×
提示
您因"违规操作"
具体请查看互助需知
我知道了
×
提示
现在去查看 取消
×
提示
确定
0
微信
客服QQ
Book学术公众号 扫码关注我们
反馈
×
意见反馈
请填写您的意见或建议
请填写您的手机或邮箱
已复制链接
已复制链接
快去分享给好友吧!
我知道了
×
扫码分享
扫码分享
Book学术官方微信
Book学术文献互助
Book学术文献互助群
群 号:481959085
Book学术
文献互助 智能选刊 最新文献 互助须知 联系我们:info@booksci.cn
Book学术提供免费学术资源搜索服务,方便国内外学者检索中英文文献。致力于提供最便捷和优质的服务体验。
Copyright © 2023 Book学术 All rights reserved.
ghs 京公网安备 11010802042870号 京ICP备2023020795号-1