Fracture of a Rail Arising From Flame-Cutting

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Abstract

To permit bolting of a 90 lb/yd. flat-bottomed rail to a steel structure, rectangular slots 2 in. wide x 1 in. deep were flame-cut in the base of the rail at 2 ft intervals to suit existing bolt holes. During subsequent handling, one of the rails (which were about 25 ft long) was dropped from a height of approximately 6 ft on to a concrete floor and it fractured into 11 pieces, each break occurring at a slot. The sample piece submitted for examination showed a wholly brittle fracture at each end, the fractures having originated at the sharp corners of the slots. During flame-cutting, a narrow band of material on each side of the cut was raised above the hardening temperature. When the torch had passed the rate of abstraction of heat from this zone by conduction into the cold mass of the rail was sufficiently rapid to amount to a quench and thus cause local hardening. The steel in the regions of the slots possessed little capacity for deformation, and fracturing of the martensitic layer, under cooling or impact stresses, would be likely to occur. The slots should have been cut mechanically.
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钢轨因火焰切割而断裂
允许90磅/码的螺栓连接。平底钢轨为钢结构,矩形槽口2英寸。宽x 1英寸。为了适应现有的螺栓孔,在轨道的底部以2英尺的间隔进行了深火焰切割。在随后的处理过程中,其中一根铁轨(约25英尺长)从大约6英尺的高度掉到混凝土地板上,断裂成11段,每段都发生在一个槽处。提交检查的样品显示两端完全呈脆性断裂,断裂起源于槽的尖角。在火焰切割过程中,切割两侧的狭窄材料带升高到硬化温度以上。当火炬通过时,通过传导将热量从该区域抽离到钢轨的冷质量中的速度足够快,足以达到淬火,从而导致局部硬化。槽区钢的变形能力很小,在冷却或冲击应力作用下,马氏体层很可能发生断裂。这些槽应该是机械切割的。
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