Fatigue Failure of a Diesel Engine Crankshaft

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Abstract

The crankshaft of a six cylinder, 225-hp diesel engine driving a small locomotive was examined. About nine months after installation a fall in oil pressure was traced to damage to No. 5 crank pin bearing. A small lip present on one side of the discontinuity apparently served to scrape the bearing material. The defect was stoned smooth, a new bearing fitted, and the engine returned to service. The engine performed satisfactorily for a further twelve months until fracture of the crankshaft through the No. 5 crank pin supervened. The fracture revealed a complex torsional fatigue failure. Microscopic examination revealed that the pin had been hard chromium plated and that the plating followed the curved edge of the outer extremity of the defect. This crank pin contained an inherent defect in the form of a slag inclusion or crack situated at the surface. That the crack only showed itself after a period of service suggests that initially it may have been slightly below the surface of the machined pin and some slight extension outwards took place in service.
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柴油机曲轴的疲劳失效
对一台驱动小型机车的225马力六缸柴油机的曲轴进行了校核。安装大约9个月后,由于5号曲柄销轴承损坏,导致油压下降。在不连续面一侧出现的小唇显然是用来刮擦轴承材料的。用石头把这个缺陷磨平,装上一个新轴承,发动机重新投入使用。在接下来的12个月里,发动机的表现令人满意,直到5号曲柄销发生曲轴断裂。断裂表现为复杂的扭转疲劳破坏。显微检查显示,针已镀硬铬,镀沿弯曲边缘的外缘的缺陷。这个曲柄销含有一个固有的缺陷,其形式是位于表面的夹渣或裂纹。裂纹是在使用一段时间后才出现的,这表明裂纹最初可能在加工销的表面以下,在使用过程中向外轻微延伸。
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