First Implementation of Ultra High Compressive Strength 12.5 ppg Cement Slurry in Production String in Kuwait Oilfields

M. Thanaa, Anwar Almihdawi, Ezequias Lopez, Ashish Fadtare, Mohammed Fauzan Ansari, Altaf Al-Shammari, K. Al-Failkawi, M. Al-Khaldy, A. Hussein, Pattan Kp Majeedkhan, Mohamed Khamis
{"title":"First Implementation of Ultra High Compressive Strength 12.5 ppg Cement Slurry in Production String in Kuwait Oilfields","authors":"M. Thanaa, Anwar Almihdawi, Ezequias Lopez, Ashish Fadtare, Mohammed Fauzan Ansari, Altaf Al-Shammari, K. Al-Failkawi, M. Al-Khaldy, A. Hussein, Pattan Kp Majeedkhan, Mohamed Khamis","doi":"10.2523/iptc-23104-ea","DOIUrl":null,"url":null,"abstract":"\n Quality Cementation across production sections consisting of depleted/weaker formations is the main challenge in Kuwait. Usage of conventional cement slurry over 15.8 ppg will lead to losses and poor zonal isolation. Newly designed 12.5 ppg enhanced compressive strength cement slurry was proposed to achieve desired zonal isolation and well integrity while avoiding losses and unnecessary remedial jobs.\n Strategy was formulated to minimize exposure of weaker formations for higher ECDs during cementation. Conventional 15.8PPG tail slurry was replaced with 12.5PPG Ultra high compressive strength (4000psi) cement slurry. New slurry design helped to carry out cementation job without any losses while achieving rapid compressive strength and excellent cement bond across production casing. The technology is based on three radical changes in the conventional way of designing cement Slurry of Substitution of part of the cement volume with inert agents of low specific weight, High packing density using solids of different sizes, and Reduction of water volume required.\n The job was performed safely and successfully, no losses was observed during and after the cementing job while getting pure cement returns at surface during both stages of cement job. CBL/VDL was performed 24 hrs after the cement job; and the results were excellent. The main advantages of this technology are: Ø High resistance to compression: Once the slurry has set, it is capable of developing compressive strength values ​​similar to heavier conventional slurry. Ø Low reactivity: Most of the elements used are chemically inert, this facilitates the design of the slurry by reducing adverse chemical reactions. Ø Low Shrinkage of Cement: Due to the reduction of the volume of the Portland cement in the slurry, the shrinkage of the set cement is reduced, which allows a better adherence of this to the formation and to the Casing. Ø Mix-ability: Does not require special equipment for its preparation, as if foamed cements require it.\n Three case histories will be presented with all data and evidence, showing design phase, planning phase, execution phase and results obtained with all logs were showing the excellent results were achieved. This technology has several applications in the industry, which can be executed satisfactorily.","PeriodicalId":283978,"journal":{"name":"Day 1 Wed, March 01, 2023","volume":"6 1","pages":"0"},"PeriodicalIF":0.0000,"publicationDate":"2023-02-28","publicationTypes":"Journal Article","fieldsOfStudy":null,"isOpenAccess":false,"openAccessPdf":"","citationCount":"0","resultStr":null,"platform":"Semanticscholar","paperid":null,"PeriodicalName":"Day 1 Wed, March 01, 2023","FirstCategoryId":"1085","ListUrlMain":"https://doi.org/10.2523/iptc-23104-ea","RegionNum":0,"RegionCategory":null,"ArticlePicture":[],"TitleCN":null,"AbstractTextCN":null,"PMCID":null,"EPubDate":"","PubModel":"","JCR":"","JCRName":"","Score":null,"Total":0}
引用次数: 0

Abstract

Quality Cementation across production sections consisting of depleted/weaker formations is the main challenge in Kuwait. Usage of conventional cement slurry over 15.8 ppg will lead to losses and poor zonal isolation. Newly designed 12.5 ppg enhanced compressive strength cement slurry was proposed to achieve desired zonal isolation and well integrity while avoiding losses and unnecessary remedial jobs. Strategy was formulated to minimize exposure of weaker formations for higher ECDs during cementation. Conventional 15.8PPG tail slurry was replaced with 12.5PPG Ultra high compressive strength (4000psi) cement slurry. New slurry design helped to carry out cementation job without any losses while achieving rapid compressive strength and excellent cement bond across production casing. The technology is based on three radical changes in the conventional way of designing cement Slurry of Substitution of part of the cement volume with inert agents of low specific weight, High packing density using solids of different sizes, and Reduction of water volume required. The job was performed safely and successfully, no losses was observed during and after the cementing job while getting pure cement returns at surface during both stages of cement job. CBL/VDL was performed 24 hrs after the cement job; and the results were excellent. The main advantages of this technology are: Ø High resistance to compression: Once the slurry has set, it is capable of developing compressive strength values ​​similar to heavier conventional slurry. Ø Low reactivity: Most of the elements used are chemically inert, this facilitates the design of the slurry by reducing adverse chemical reactions. Ø Low Shrinkage of Cement: Due to the reduction of the volume of the Portland cement in the slurry, the shrinkage of the set cement is reduced, which allows a better adherence of this to the formation and to the Casing. Ø Mix-ability: Does not require special equipment for its preparation, as if foamed cements require it. Three case histories will be presented with all data and evidence, showing design phase, planning phase, execution phase and results obtained with all logs were showing the excellent results were achieved. This technology has several applications in the industry, which can be executed satisfactorily.
查看原文
分享 分享
微信好友 朋友圈 QQ好友 复制链接
本刊更多论文
科威特油田首次在生产管柱中使用超高抗压强度12.5 ppg水泥浆
在科威特,高质量的固井是主要的挑战。使用超过15.8 ppg的常规水泥浆会导致漏失和层间隔离效果差。新设计的12.5 ppg抗压强度增强水泥浆可以达到理想的层间隔离和井的完整性,同时避免损失和不必要的补救工作。制定的策略是为了在固井期间最大限度地减少对较弱地层的暴露,以获得较高的ecd。常规的15.8PPG尾浆被12.5PPG超高抗压强度(4000psi)水泥浆取代。新的泥浆设计有助于在没有任何损失的情况下进行固井作业,同时在生产套管上实现快速抗压强度和优异的水泥胶结。该技术是基于对传统水泥浆设计方式的三个根本性改变:用低比重的惰性剂替代部分水泥体积,使用不同尺寸的固体来提高充填密度,减少所需的水量。作业安全、成功,在固井作业期间和之后都没有观察到漏失,在两阶段的固井作业中都获得了纯净的地面水泥。固井作业后24小时进行CBL/VDL;结果非常好。该技术的主要优点是:Ø高抗压性:一旦浆料凝固,它能够形成与较重的常规浆料相似的抗压强度值。Ø低反应性:大多数使用的元素是化学惰性的,这有利于浆料的设计,减少不良的化学反应。Ø水泥的低收缩率:由于水泥浆中硅酸盐水泥的体积减少,水泥的收缩率降低,这使得水泥与地层和套管的粘附性更好。Ø混合性:不需要特殊的设备来制备,就像泡沫水泥需要它一样。三个案例历史将展示所有的数据和证据,显示设计阶段,计划阶段,执行阶段和结果,所有日志都显示了取得的优异结果。该技术在工业上有多种应用,并取得了满意的效果。
本文章由计算机程序翻译,如有差异,请以英文原文为准。
求助全文
约1分钟内获得全文 去求助
来源期刊
自引率
0.00%
发文量
0
期刊最新文献
The Proper Well Spacings – A Supplementary Method to Maximize The Gulf of Thailand Development Project Value Seismic Driven Machine Learning to Improve Precision and Accelerate Screening Shallow Gas Potentials in Tunu Shallow Gas Zone, Mahakam Delta, Indonesia Rejuvenating Waterflood Reservoir in a Complex Geological Setting of a Matured Brown Field Intelligent Prediction of Downhole Drillstring Vibrations in Horizontal Wells by Employing Artificial Neural Network Sand Fill Clean-Out on Wireline Enables Access to Additional Perforation Zones in Gas Well Producer
×
引用
GB/T 7714-2015
复制
MLA
复制
APA
复制
导出至
BibTeX EndNote RefMan NoteFirst NoteExpress
×
×
提示
您的信息不完整,为了账户安全,请先补充。
现在去补充
×
提示
您因"违规操作"
具体请查看互助需知
我知道了
×
提示
现在去查看 取消
×
提示
确定
0
微信
客服QQ
Book学术公众号 扫码关注我们
反馈
×
意见反馈
请填写您的意见或建议
请填写您的手机或邮箱
已复制链接
已复制链接
快去分享给好友吧!
我知道了
×
扫码分享
扫码分享
Book学术官方微信
Book学术文献互助
Book学术文献互助群
群 号:481959085
Book学术
文献互助 智能选刊 最新文献 互助须知 联系我们:info@booksci.cn
Book学术提供免费学术资源搜索服务,方便国内外学者检索中英文文献。致力于提供最便捷和优质的服务体验。
Copyright © 2023 Book学术 All rights reserved.
ghs 京公网安备 11010802042870号 京ICP备2023020795号-1