Low Cost Plug and Abandonment with Hybrid Hydraulic Pulling Unit

Tengku Khairul Izwan Tengku Ahmad, Abdul Hanif Abdullah
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Abstract

Plug and Abandonment (P&A) operations with conventional Hydraulic Workover Unit (WHU) have an enormous benefit and impact on low-cost P&A campaign in Malaysia compare with using conventional drilling rig. Subsequently, this Hybrid Hydraulic Pulling Unit (HHPU) was the first successful deployed and safely delivered for P&A campaign together with conductor removal in offshore West Malaysia. This paper presents case study that showcase the capability of HHPU for low-cost permanent P&A campaign by eliminate requirement for additional bringing rigging-up and rigging-down of casing jack unit for conductor removal operation. The unit manage to cut and pull-out the existing completion strings, setting cement plugs, cut and pull-out multiple strings of casing along with retrieving the 24″ conductors delivering the most advantageous outcome for P&A campaign safely, efficiently and cost effectively. It was invented from 340K HWU with improvise features that capable of pull-out existing completion string and removal of the conductor with size up to 36″. This paper demonstrates a unique combination of techniques and equipment of a successfully low-cost P&A operation with excellent client satisfaction with no incident and accident were recorded. The end results may contradict traditional P&A methods, but the case history can be used for future reference or potential replication in South East Asia region.
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采用混合液压拉拔装置的低成本桥塞和弃井
在马来西亚,与使用常规钻机相比,使用传统液压修井装置(WHU)进行封井弃井(P&A)作业具有巨大的优势和影响。随后,该混合液压拉拔装置(HHPU)在西马来西亚海上的P&A作业中首次成功部署,并安全交付。本文通过案例研究,展示了HHPU在低成本的永久性弃井作业中的能力,因为它消除了在拆除导体作业中对套管千顶装置进行额外起吊和下吊的要求。该装置能够切割和取出现有的完井管柱,坐封水泥塞,切割和取出多套套管,同时回收24根″套管,为封堵和弃井作业提供了最有利的结果,安全、高效、经济。它是由340K HWU发明的,具有即兴功能,能够拔出现有的完井管柱并移除尺寸达36的导体″。本文展示了一种独特的技术和设备组合,成功实现了低成本的弃井作业,客户满意度极高,没有发生任何事故。最终结果可能与传统的P&A方法相矛盾,但该案例历史可用于未来参考或东南亚地区的潜在复制。
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