Possibilities Study of a Non-condensable Gas Exhaust System through the Condensate Injection Pipe at PLTP Wayang Windu

Annisa Nurlatifah, Anton Purwakusumah
{"title":"Possibilities Study of a Non-condensable Gas Exhaust System through the Condensate Injection Pipe at PLTP Wayang Windu","authors":"Annisa Nurlatifah, Anton Purwakusumah","doi":"10.25299/jgeet.2023.8.02-2.13878","DOIUrl":null,"url":null,"abstract":"Wayang Windu Geothermal Power Plant, located in Pangalengan, Bandung regency, West Java with an installed capacity of 227 MWe has two units to generate electricity and deliver to the Jawa, Madura, and Bali grid. The steam extracted from the reservoir contains non-condensable gas of about 1-1.2% of total steam extracted, with the gas composition is CO2 92%, H2S 2%, NH3 0.1%, and residual gasses 4.9%. Possibilities study of a non-condensable gas exhaust through the condensate injection pipe was created as the efforts in the environmental conservation aspect for reducing carbon released to the atmosphere and reinjected back into the reservoir. This study was simulated in Wayang Windu Unit 2 by calculating the non-condensable gas flow rate from the gas removal system into the condensate injection pipe near of cooling tower blowdown power station area. The analysis result of this study indicates that the non-condensable gas requires a higher flow rate of condensate to dissolve the entire non-condensable gas, and may cause the slug flow pattern which would endanger the condensate pipeline system also destabilize the non-condensable gas exhaust operation process from the condenser through the gas removal system. To deal with this problem, the possibility of exhausting the non-condensable gas produced by the gas removal system can be alternated by flowing its non-condensable gas into a flash absorber system and converting its non-condensable gas into other eco-friendly products and power plant safe.","PeriodicalId":31931,"journal":{"name":"JGEET Journal of Geoscience Engineering Environment and Technology","volume":null,"pages":null},"PeriodicalIF":0.0000,"publicationDate":"2023-07-31","publicationTypes":"Journal Article","fieldsOfStudy":null,"isOpenAccess":false,"openAccessPdf":"","citationCount":"0","resultStr":null,"platform":"Semanticscholar","paperid":null,"PeriodicalName":"JGEET Journal of Geoscience Engineering Environment and Technology","FirstCategoryId":"1085","ListUrlMain":"https://doi.org/10.25299/jgeet.2023.8.02-2.13878","RegionNum":0,"RegionCategory":null,"ArticlePicture":[],"TitleCN":null,"AbstractTextCN":null,"PMCID":null,"EPubDate":"","PubModel":"","JCR":"","JCRName":"","Score":null,"Total":0}
引用次数: 0

Abstract

Wayang Windu Geothermal Power Plant, located in Pangalengan, Bandung regency, West Java with an installed capacity of 227 MWe has two units to generate electricity and deliver to the Jawa, Madura, and Bali grid. The steam extracted from the reservoir contains non-condensable gas of about 1-1.2% of total steam extracted, with the gas composition is CO2 92%, H2S 2%, NH3 0.1%, and residual gasses 4.9%. Possibilities study of a non-condensable gas exhaust through the condensate injection pipe was created as the efforts in the environmental conservation aspect for reducing carbon released to the atmosphere and reinjected back into the reservoir. This study was simulated in Wayang Windu Unit 2 by calculating the non-condensable gas flow rate from the gas removal system into the condensate injection pipe near of cooling tower blowdown power station area. The analysis result of this study indicates that the non-condensable gas requires a higher flow rate of condensate to dissolve the entire non-condensable gas, and may cause the slug flow pattern which would endanger the condensate pipeline system also destabilize the non-condensable gas exhaust operation process from the condenser through the gas removal system. To deal with this problem, the possibility of exhausting the non-condensable gas produced by the gas removal system can be alternated by flowing its non-condensable gas into a flash absorber system and converting its non-condensable gas into other eco-friendly products and power plant safe.
查看原文
分享 分享
微信好友 朋友圈 QQ好友 复制链接
本刊更多论文
大阳窗PLTP凝结水注管非凝结水排气系统的可行性研究
Wayang Windu地热发电厂位于西爪哇万隆县的Pangalengan,装机容量为227兆瓦,有两台机组发电,并提供给爪哇、马杜拉和巴厘岛电网。储层抽汽含不凝性气体约占抽汽总量的1-1.2%,气体成分为CO2 92%, H2S 2%, NH3 0.1%,残余气体4.9%。通过凝析油注入管道进行非凝析气体排放的可能性研究,是为了减少释放到大气中并重新注入储层的碳,从而保护环境。本研究以大阳温都2号机组为例进行了数值模拟,计算了除气系统进入冷却塔排污电站区域附近凝结水喷射管的不凝气体流量。本研究的分析结果表明,不凝性气体需要较高的凝结水流量才能溶解全部不凝性气体,并且可能产生段塞流态,危及凝结水管道系统,也会使不凝性气体从冷凝器经除气系统排出运行过程不稳定。为了解决这个问题,可以通过将气体去除系统产生的不可冷凝气体输送到闪蒸吸收系统中,并将其不可冷凝气体转化为其他环保产品和发电厂安全的方式来交替使用。
本文章由计算机程序翻译,如有差异,请以英文原文为准。
求助全文
约1分钟内获得全文 去求助
来源期刊
自引率
0.00%
发文量
6
审稿时长
16 weeks
期刊最新文献
Geomorphology and Geology Studies Using Digital Elevation Model (DEM) Data In the Watershed Area of Kampar Regency, Riau Province Geological Analysis for Slope Stability Using the Rock Structure Rating (RSR) Method and Atterberg Limit at Riau - West Sumatra Cross road Km 165 Harau Subdistrict, Lima puluh Kota Regency, West Sumatra Province Economic And Sensitivity Analysis Stimulation Of Coiled Tubing And Bullhead Combination On A Horizontal Well The Effect of Vermicompost Fertilizer and Mutiara Npk 16:16:16 on the Growth and Production of Pakcoy Plant (Brassica Rapa L.) The Effect of Sales Growth, Dividend Policy and Return on Assets on Debt Policy in Property and Real Estate Companies Listed on the Indonesia Stock Exchange in 2013 - 2017
×
引用
GB/T 7714-2015
复制
MLA
复制
APA
复制
导出至
BibTeX EndNote RefMan NoteFirst NoteExpress
×
×
提示
您的信息不完整,为了账户安全,请先补充。
现在去补充
×
提示
您因"违规操作"
具体请查看互助需知
我知道了
×
提示
现在去查看 取消
×
提示
确定
0
微信
客服QQ
Book学术公众号 扫码关注我们
反馈
×
意见反馈
请填写您的意见或建议
请填写您的手机或邮箱
已复制链接
已复制链接
快去分享给好友吧!
我知道了
×
扫码分享
扫码分享
Book学术官方微信
Book学术文献互助
Book学术文献互助群
群 号:481959085
Book学术
文献互助 智能选刊 最新文献 互助须知 联系我们:info@booksci.cn
Book学术提供免费学术资源搜索服务,方便国内外学者检索中英文文献。致力于提供最便捷和优质的服务体验。
Copyright © 2023 Book学术 All rights reserved.
ghs 京公网安备 11010802042870号 京ICP备2023020795号-1