Heat recovery from a spray dryer using a run-around coil system

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Abstract

This project at Clayton Aniline Co. (CAC) demonstrates the use of a finned-tube heat exchanger and run-around coil system to recovery heat from a spray-dryer exhaust to pre-heat the inlet air. It was originally envisaged that this would reduce the energy consumption of the dryer by 12%, equivalent to 9.4 therms/h.

Funding was granted by the Energy Efficiency Office of the Department of Energy under the Energy Efficiency Demonstration Scheme for the installation and monitoring of the project. This project is one of a package of demonstrations for heat recovery in spray dryers. A parallel project at ABM Chemicals uses a glass tube heat exchanger to recover energy from the dryer exhaust, and a further project at BIP Chemicals demonstrates the use of a separate heat source to pre-heat the dryer inlet air.

Within the U.K., widespread adoption of heat recovery on spray dryers would lead to energy savings of 2,500 TJ/yr or 100,000 tonnes of coal equivalent (tce)/yr. It is estimated that, within the next 5 yr, around 20% of this will be achieved, resulting in savings of around 20,000 tce/yr, worth £1.6 million yr.

The heat recovery system was installed at CAC in July 1982. Unfortunately, due to the built-up of solids on the fins, the unit had to be removed after only three days operation. The equipment was therefore modified and the changes included:

reducing the number of fins from from 8/in. to 4/in.: this reduction in are meand a 30% loss of potential savings;

improving the exchanger spray wash system by including an additional row of nozzles directed towards the centre of the unit.

The replacement exchanger was installed in July 1984 and, since that time, has operated satisfactoryly. It has not adversely affected the operation of the spray dryer, as the problems of excessive solids deposition and ineffective washing have now been overcome.

Detailed monitoring has not yet been completed, but preliminary information and design calculations estimate that for the modified exchanger, energy savings averaging 6.5 therms/h (191 kW) are probable. These are worth about £17,200 to CAC and hence the payback period on the installation cost of £35,200 is 2 yr.

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使用绕线系统从喷雾干燥器回收热量
克莱顿苯胺公司(CAC)的这个项目演示了使用翅片管换热器和绕线盘管系统从喷雾干燥器排气中回收热量,以预热进气。最初设想,这将使干燥机的能耗减少12%,相当于9.4 therms/h。能源部能源效率办公室根据能源效率示范计划为该项目的安装和监测提供了资金。该项目是喷雾干燥器热回收示范项目之一。ABM Chemicals的一个平行项目使用玻璃管换热器从干燥器排气中回收能量,而BIP Chemical的另一个项目演示了使用单独的热源来预热干燥器入口空气。在英国,在喷雾干燥器上广泛采用热回收将导致每年2500 TJ或100000吨煤当量(tce)的节能。据估计,在未来5年内,将实现约20%的目标,从而每年节省约20000吨标煤当量,价值160万英镑。热回收系统于1982年7月在CAC安装。不幸的是,由于翅片上堆积了固体,该装置仅运行了三天就不得不拆除。因此,对设备进行了修改,更改包括:将翅片数量从8/in减少。至4/in.:这意味着潜在储蓄损失了30%;通过包括指向单元中心的附加喷嘴排来改进交换器喷雾洗涤系统。更换的交换器于1984年7月安装,从那时起,运行情况令人满意。它没有对喷雾干燥器的操作产生不利影响,因为现在已经克服了固体沉积过多和洗涤无效的问题。详细的监测尚未完成,但初步信息和设计计算估计,对于改造后的交换器,可能会节省平均6.5 therms/h(191 kW)的能源。这些对CAC来说价值约17200英镑,因此35200英镑的安装成本回收期为2年。
本文章由计算机程序翻译,如有差异,请以英文原文为准。
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