First Application of Coiled Hose in Indonesia and First Deployment of Coiled Hose with Roller Boogies in the World to Access Highly Deviated Well

Gerardus Putra Pancawisna, R. Hidayat, G. D. Dahnil, Risal Rahman, P. S. Kurniawati, R. Marindha, K. Umar, _. Ferdian, Irwan Setyaji, Muhammad Masrur, Stian Steinsholm
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Abstract

The paper is aimed to present the engineering design and execution of first application of coiled hose in Indonesia to perform nitrogen unload including its first deployment with roller boogies in the world to tackle the challenge of highly deviated well. The new well of XX-107 was completed with 2 (two) gravel pack zones and tubingless section. In order to produce the well from the gravel pack zones, completion fluid, which filled in the XX-107 well, should be displaced to ensure underbalance condition once the SSDs of those gravel pack zones were opened. After comparing several available methods, coiled hose was chosen to perform nitrogen unload due to its compact and lightweight nature in comparison to conventional coiled tubing. Coiled hose enabled seamless deployment right after the well was completed by the workover unit. Furthermore, the maximum deviation of 84 deg in XX-107 well provided additional challenge to access the well since coiled hose was gravity feed. Several simulations were performed and they resulted in the utilization of roller boogies to minimize friction during RIH and increase the reach of coiled hose in this well. As a result, this operation achieved its main objective of displacing the completion fluid out of the well and created underbalance condition in front of the gravel pack zones. Although the efficiency was only 67.5%, it managed to create 1071 psi of underbalance value and consequently the well flowed at 8 MMscfd. Its lightweight nature was like electricline unit and it consumed less space on the upper deck of the platform. Moreover, the deployment and setup process was performed offline which optimized the operating time event further. The cumulative operating time was only 13 hours including demobilization process while in terms of logistic coiled hose only required 1 trip whereas coiled tubing unit required at least 3 trips. Lastly, this operation requires only 10 personnel for 24-hr operation in comparison to 15 coiled tubing personnel which meant, in this Covid-19 pandemic, provided less risky solution.
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印度尼西亚首次使用螺旋软管,世界上首次使用带滚轮转向器的螺旋软管进入大斜度井
本文旨在介绍在印度尼西亚首次应用连续软管进行氮气卸载的工程设计和实施,包括在世界上首次使用滚轮转向器来解决大斜度井的挑战。XX-107新井完成了2个砾石充填层和无油管段。为了从砾石充填层进行生产,在打开砾石充填层的ssd后,应将填充在XX-107井中的完井液置换,以确保处于欠平衡状态。在比较了几种可用的方法后,由于与传统的连续油管相比,连续软管结构紧凑,重量轻,因此选择了连续软管进行氮气卸载。在修井装置完成完井后,连续软管即可实现无缝部署。此外,XX-107井的最大斜度为84度,由于连续软管是重力供给的,这给下入井带来了额外的挑战。进行了多次模拟,结果表明,使用滚轮转向器可以最大限度地减少RIH过程中的摩擦,并增加连续软管在该井中的延伸范围。因此,该作业实现了将完井液排出井外的主要目标,并在砾石充填层前产生了欠平衡状态。尽管效率只有67.5%,但它还是产生了1071 psi的欠平衡值,因此井的流量为800万立方英尺/天。它的重量轻,就像电线一样,在平台的上层占用的空间更少。此外,部署和设置过程离线进行,进一步优化了操作时间事件。包括复员过程在内,累计作业时间仅为13小时,而在物流方面,连续软管只需要一次下钻,而连续油管单元至少需要3次下钻。最后,与15名连续油管人员相比,该操作只需要10名人员进行24小时操作,这意味着,在Covid-19大流行期间,提供了风险较低的解决方案。
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