Unconventional Approach to Managing Kick During Gas Well Drilling

K. Hannah, Maku Gbenga, Ike Micheal, Olagunju Khalid, Ojo Olaniyi, O. James
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引用次数: 2

Abstract

Interruption in drilling operation occurs when drilling bit penetrates permeable gas sand with formation pressure greater than the pressure exerted by the drilling fluid in use. Consequently, due to pressure imbalance, there is an extraneous influx of gas into the wellbore, which would bring the drilling progress to a stop as it is necessary to restore pressure/fluid equilibrium throughout the system to contain the kick. This study presents a case study where a gas kick was unconventionally managed. While drilling 8 ½" hole at 11,682 ft, a mud gush shooting up through the rotary table to the stabbing board was observed. In attempt to shut-in the well, an accidental shear of the pipe at the surface occurred with the top of fish at 51 ft and with no means of circulating out the influx from the bottom of the well. Due to the well control issue, the cut pipe could not be reached to mill the top of the fish, prior to engaging same. The well was therefore put under control employing Lubricate and Bleed (LB) approach, which is a well control procedure applied in peculiar cases or situation, this is a method or procedure of removing gas in hole when there is no possible way of circulation. The sheared pipe located at about 52 ft below rotary, the Top Of fish was dressed from 51ft to 52ft and the string was eventually severed at 11460 ft, the rest 222 ft of fish was recovered using Overshot, Burn Shoe and Wash-Over assembly. With the effective application of the LB approach, the well was restored, and fish recovered within a relatively short period of time such that values weren't eroded. The approach employed in this study could be applied in a case of accidental shearing of the pipe such that the whole drilling progress is not brought to a total stop. The consequence of not exploring this approach is an additional cost of drilling a sidetrack well or totally abandoning the well. This paper can be used as a training tool to sharpen and build confidence in tackling well control using volumetric bleeding method. As this method is rare, and not simulated for during most well control certification exercises, it will be beneficial to a practicing engineer and can reduce some of the errors that could occur in a rare case of sheared pipe / well control.
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气井钻井过程中控制井涌的非常规方法
当地层压力大于所使用的钻井液压力时,钻头穿过可渗透气砂,导致钻井作业中断。因此,由于压力不平衡,会有外来的气体流入井筒,这将导致钻井进程停止,因为必须在整个系统中恢复压力/流体平衡,以遏制溢流。本研究介绍了一个非常规管理气涌的案例研究。在11682英尺处钻8.5英寸的井眼时,观察到泥浆通过转盘涌向刺入板。在试图关井的过程中,发生了一次意外的地面管柱剪切事故,此时截尾器的顶部距离井底51英尺,无法将井底的溢流循环出来。由于井控问题,切割后的管柱无法在接合渔获器之前磨碎渔获器的顶部。因此,采用润滑和放气(LB)方法对该井进行了控制,这是一种适用于特殊情况或情况的井控程序,它是在无法循环的情况下清除井内气体的方法或程序。剪切管柱位于旋转管下方约52英尺处,在51英尺至52英尺处进行了修整,最终在11460英尺处切断了管柱,使用Overshot、Burn Shoe和Wash-Over组合回收了其余222英尺的渔获。由于LB方法的有效应用,该井得到了修复,鱼在相对较短的时间内被回收,因此价值没有被侵蚀。本研究中采用的方法可以应用于意外剪切管道的情况,使整个钻井过程不会完全停止。不采用这种方法的后果是钻井侧钻井或完全弃井的额外成本。本文可以作为一种培训工具,提高和建立使用体积放血方法进行井控的信心。由于这种方法很少见,并且在大多数井控认证过程中都没有进行模拟,因此对于实践工程师来说是有益的,并且可以减少在罕见的剪切管/井控情况下可能发生的一些错误。
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