New Approaches for Drilling Highly Depleted Reservoir in Deep Water Wells

Ola Balbaa, Hesham Mohamed, S. Elkholy, Mohamed ElRashidy, R. Munger, M. Najwani
{"title":"New Approaches for Drilling Highly Depleted Reservoir in Deep Water Wells","authors":"Ola Balbaa, Hesham Mohamed, S. Elkholy, Mohamed ElRashidy, R. Munger, M. Najwani","doi":"10.2118/207779-ms","DOIUrl":null,"url":null,"abstract":"\n While drilling highly depleted gas reservoirs with a very narrow drilling window, Common drilling methods like utilizing loss of circulation pills, wellbore strengthening materials and managed pressure drilling (MPD) are being used in several reservoirs, yet it cannot be successful or cost effective if applied in a traditional manner.\n Innovative approaches to enable drilling wells in highly depleted reservoir in the Mediterranean deep water were adopted. The approaches incorporated design changes to the well and Bottom hole assembly (BHA), optimized drilling practices, and unconventional use of MPD while drilling and cementing production liner.\n Well design change in comparison to offset wells to allow drilling the reservoir in one hole section. Several design changes were considered in the BHA and drilling fluids to prevent as well as mitigate losses and differential sticking risks. From the BHA viewpoint, one of the key successful prevention measures was maximizing the standoff to reduce the contact area with the formation, this was achieved through utilizing spiral heavy wall drill pipe (HWDP) instead of drill collars in addition to a modeled placement of stabilizers and roller reamers. While on the drilling fluid side, Calcium carbonate material was added to strengthen wellbore, prevent losses and avoid formation damage. Particle size up to 1000 micron and concentration up to 40ppb was used to strengthen the depleted sands dynamically while drilling. Furthermore, as mitigation to stuck pipe, Jar and accelerator placement was simulated to achieve optimum impulse and impact force while maintaining the Jar above potential sticking zone. Whereas to address the consequence of a stuck pipe event, disconnect subs were placed in BHA to allow for recovering the drill string efficiently.\n MPD was first introduced in the Mediterranean in 2007 and continued to develop this well-known technique to mitigate various drilling challenges. For this well, MPD was one of the key enabling factors to safely drill, run and cement the production liner.\n Surface back pressure MPD allowed using the lowest possible mud weight in the hole and maintaining downhole pressure constant in order to manage the narrow drilling window between the formation pressure and fracture pressure (less than 0.4 ppg). MPD was also applied for the first time for running and cementing the production liner to prevent losses and achieve good cement quality which is a key to successful well production.","PeriodicalId":10959,"journal":{"name":"Day 3 Wed, November 17, 2021","volume":null,"pages":null},"PeriodicalIF":0.0000,"publicationDate":"2021-12-09","publicationTypes":"Journal Article","fieldsOfStudy":null,"isOpenAccess":false,"openAccessPdf":"","citationCount":"0","resultStr":null,"platform":"Semanticscholar","paperid":null,"PeriodicalName":"Day 3 Wed, November 17, 2021","FirstCategoryId":"1085","ListUrlMain":"https://doi.org/10.2118/207779-ms","RegionNum":0,"RegionCategory":null,"ArticlePicture":[],"TitleCN":null,"AbstractTextCN":null,"PMCID":null,"EPubDate":"","PubModel":"","JCR":"","JCRName":"","Score":null,"Total":0}
引用次数: 0

Abstract

While drilling highly depleted gas reservoirs with a very narrow drilling window, Common drilling methods like utilizing loss of circulation pills, wellbore strengthening materials and managed pressure drilling (MPD) are being used in several reservoirs, yet it cannot be successful or cost effective if applied in a traditional manner. Innovative approaches to enable drilling wells in highly depleted reservoir in the Mediterranean deep water were adopted. The approaches incorporated design changes to the well and Bottom hole assembly (BHA), optimized drilling practices, and unconventional use of MPD while drilling and cementing production liner. Well design change in comparison to offset wells to allow drilling the reservoir in one hole section. Several design changes were considered in the BHA and drilling fluids to prevent as well as mitigate losses and differential sticking risks. From the BHA viewpoint, one of the key successful prevention measures was maximizing the standoff to reduce the contact area with the formation, this was achieved through utilizing spiral heavy wall drill pipe (HWDP) instead of drill collars in addition to a modeled placement of stabilizers and roller reamers. While on the drilling fluid side, Calcium carbonate material was added to strengthen wellbore, prevent losses and avoid formation damage. Particle size up to 1000 micron and concentration up to 40ppb was used to strengthen the depleted sands dynamically while drilling. Furthermore, as mitigation to stuck pipe, Jar and accelerator placement was simulated to achieve optimum impulse and impact force while maintaining the Jar above potential sticking zone. Whereas to address the consequence of a stuck pipe event, disconnect subs were placed in BHA to allow for recovering the drill string efficiently. MPD was first introduced in the Mediterranean in 2007 and continued to develop this well-known technique to mitigate various drilling challenges. For this well, MPD was one of the key enabling factors to safely drill, run and cement the production liner. Surface back pressure MPD allowed using the lowest possible mud weight in the hole and maintaining downhole pressure constant in order to manage the narrow drilling window between the formation pressure and fracture pressure (less than 0.4 ppg). MPD was also applied for the first time for running and cementing the production liner to prevent losses and achieve good cement quality which is a key to successful well production.
查看原文
分享 分享
微信好友 朋友圈 QQ好友 复制链接
本刊更多论文
深水井高衰竭油藏钻井新方法
虽然钻井高度枯竭气藏的钻井窗口非常窄,但常用的钻井方法,如使用防漏剂、井筒强化材料和控压钻井(MPD),已经在几个油藏中得到了应用,但如果采用传统方式,这些方法并不成功,也不符合成本效益。采用创新方法在地中海深水高度枯竭的油藏中钻井。这些方法包括改变井底钻具组合(BHA)的设计,优化钻井作业,以及在钻井和固井生产尾管时非常规地使用MPD。与邻井相比,井的设计发生了变化,可以在一个井段内钻完储层。为了防止和减轻漏失和不同的卡钻风险,BHA和钻井液的设计进行了一些调整。从底部钻具组合的角度来看,成功的关键预防措施之一是最大限度地减少与地层的接触面积,这是通过使用螺旋厚壁钻杆(HWDP)来代替钻铤,以及放置稳定器和滚轮扩眼器来实现的。在钻井液方面,加入碳酸钙材料加固井筒,防止漏失,避免地层损害。颗粒尺寸可达1000微米,浓度可达40ppb,用于在钻井过程中动态强化枯竭砂。此外,为了缓解卡钻,模拟了震击器和加速器的放置,以获得最佳的冲力和冲击力,同时将震击器保持在潜在卡钻区域上方。然而,为了解决卡钻事件的后果,在BHA中放置了断开短节,以便有效地恢复钻柱。MPD于2007年首次在地中海引入,并不断发展这一众所周知的技术,以减轻各种钻井挑战。对于这口井来说,MPD是确保生产尾管安全钻进、下入和固井的关键因素之一。地面背压MPD允许使用尽可能低的井中泥浆比重,并保持井下压力恒定,以控制地层压力和破裂压力之间的狭窄钻井窗口(小于0.4 ppg)。MPD也首次应用于生产尾管的下入和固井,以防止漏失,并获得良好的水泥质量,这是成功生产的关键。
本文章由计算机程序翻译,如有差异,请以英文原文为准。
求助全文
约1分钟内获得全文 去求助
来源期刊
自引率
0.00%
发文量
0
期刊最新文献
Assessment of Unconventional Resources Opportunities in the Middle East Tethyan Petroleum System in a Transfer Learning Context Block 61 Drilling Fluids Optimization Journey High Resolution Reservoir Simulator Driven Custom Scripts as the Enabler for Solving Reservoir to Surface Network Coupling Challenges Pre-Engineered Standardized Turbomachinery Solutions: A Strategic Approach to Lean Project Management Using Active and Passive Near-Field Hydrophones to Image the Near-Surface in Ultra-Shallow Waters Offshore Abu Dhabi
×
引用
GB/T 7714-2015
复制
MLA
复制
APA
复制
导出至
BibTeX EndNote RefMan NoteFirst NoteExpress
×
×
提示
您的信息不完整,为了账户安全,请先补充。
现在去补充
×
提示
您因"违规操作"
具体请查看互助需知
我知道了
×
提示
现在去查看 取消
×
提示
确定
0
微信
客服QQ
Book学术公众号 扫码关注我们
反馈
×
意见反馈
请填写您的意见或建议
请填写您的手机或邮箱
已复制链接
已复制链接
快去分享给好友吧!
我知道了
×
扫码分享
扫码分享
Book学术官方微信
Book学术文献互助
Book学术文献互助群
群 号:481959085
Book学术
文献互助 智能选刊 最新文献 互助须知 联系我们:info@booksci.cn
Book学术提供免费学术资源搜索服务,方便国内外学者检索中英文文献。致力于提供最便捷和优质的服务体验。
Copyright © 2023 Book学术 All rights reserved.
ghs 京公网安备 11010802042870号 京ICP备2023020795号-1