Interburden Isolation & Slotted Liner Placement as Solids Control Measure to Improve Well Performance by Reducing Operating Costs and Maximising Gas Production

R. Viljoen, Vikram Sharma, S. Mazumder, A. Rajora, E. Córdova, Keith Wilson, M. Thompson
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Abstract

Solids production in coal seam gas wells have been a large contributor to down-hole completion failure in the Surat Basin, Australia. Since 2016, solids production has become an important focal point for well quality improvement for the Surat Basin operator and has focused its efforts on trying to a) understand the mechanism of pump failure related to solids, b) quantifying the origin of the solids, c) understanding where they come from geologically and d) developing best practices to optimise well designs and operating practices. This study has focused on improving drilling, completion and post-completion activities to reduce operating costs and maximise gas production. The implementation of formal procedural workflows and management of key performance indicators have formed the fundamentals for managing the delivery of quality wells through metrics such as interburden isolation, and thus reducing the risk of well impairment. Sourcing of additional equipment such as shorter slotted casing joints has increased the material limits for interburden isolation. The development of casing tally software has drastically reduced the risk of manual calculation errors and improved completions accuracy and efficiency. Solid samples have been taken from production water, completion tubing and well sumps. The samples from production water indicate that the average particle size is reduced with a reduction in fluid velocities. This inefficiency to remove the larger particles sizes coincides with a reduction in pump run-life due to settling of these solids in the tubing. An increase in periodic pump shut downs has also resulted in increased pump failure related to solids accumulation. Therefore, the optimisation of pump sizes and tubing designs plays a very important role in effective solids removal and increasing pump run-life. The average mineral composition of the solids samples may suggest that the majority of samples originate from the lower Juandah and upper Taroom formations. Further testing will be required to refine any hypothesis of solid origins and related strategies for more targeted isolation. A higher solids production correlates well with an increase in interburden exposure. The variable trends may indicate that some areas are more prone to solids production due to geological differences. Solids quantities do not demonstrate any noticeable trends over time for vertical wells but do increase over time for deviated wells. In some cases, solids quantities increase at ascending rates; this may suggest that the swellable packers are not creating effective seals and the well is washing away behind the packers and subsequently increasing the surface area of the wellbore. Through the reduction of exposed interburden, the potential risk of well impairment has been significantly reduced. Further work will be required to understand the effective use of swellable packers in deviated wells and possible strategies to overcome their shortcomings. Drilling bottom hole assembly design and changes to drilling parameters and practices have shown to improve borehole gauge to maximise the effectiveness of swellable packers. It is expected that, with a continual solids sampling program in place, a refined interpretation of solids production will be established over time, and an improved execution and operations strategy will be optimised to suit.
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层间隔离和开槽尾管放置作为固控措施,通过降低作业成本和最大化产气量来提高油井性能
在澳大利亚Surat盆地,煤层气井的固体产量是导致井下完井失败的主要原因。自2016年以来,固体产量已成为Surat盆地运营商提高井质量的重要焦点,并将努力集中在a)了解与固体相关的泵故障机制,b)量化固体的来源,c)了解它们的地质来源以及d)开发最佳实践以优化井设计和操作实践。该研究的重点是改进钻井、完井和完井后作业,以降低作业成本,最大限度地提高天然气产量。正式程序工作流程的实施和关键绩效指标的管理,为通过层间隔离等指标管理优质油井的交付奠定了基础,从而降低了油井受损的风险。采购额外的设备,如较短的开槽套管接头,增加了层间隔离的材料限制。套管理货软件的开发大大降低了人工计算错误的风险,提高了完井精度和效率。从生产水、完井油管和井池中采集了固体样品。采出水样品表明,随着流体速度的降低,平均粒径减小。这种去除较大颗粒的效率低下,同时由于这些固体在油管中的沉淀,泵的运行寿命也会缩短。定期关闭泵的次数增加也导致与固体堆积相关的泵故障增加。因此,泵尺寸和油管设计的优化在有效去除固体和延长泵的运行寿命方面起着非常重要的作用。固体样品的平均矿物组成可能表明,大多数样品来自Juandah下部和Taroom上部地层。将需要进一步的测试来完善任何关于可靠起源的假设和更有针对性的隔离的相关策略。较高的固体产量与层间暴露量的增加密切相关。变化趋势可能表明,由于地质差异,某些地区更容易产生固体。对于直井,固相量没有明显的变化趋势,但对于斜井,固相量会随着时间的推移而增加。在某些情况下,固体数量以递增的速率增加;这可能表明膨胀封隔器没有产生有效的密封,井被冲刷到封隔器后面,从而增加了井筒的表面积。通过减少暴露的夹层,油井受损的潜在风险显著降低。进一步的工作需要了解可膨胀封隔器在斜度井中的有效应用,以及克服其缺点的可能策略。井底钻具组合的设计以及钻井参数的变化和实践表明,可以改善井眼尺寸,最大限度地提高可膨胀封隔器的有效性。预计,随着持续的固体取样程序的实施,随着时间的推移,将建立一个精确的固体产量解释,并改进执行和操作策略,以适应。
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