Smart Upgrades to Maximize the Use of Existing Produced Water Treatment Facilities for CEOR

S. Grottendorfer, R. Kadnar, Günter Staudigl
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引用次数: 2

Abstract

The maximum use of existing surface produced water treatment (PWT) facilities is a prerequisite for an economic chemical enhanced oil recovery (cEOR) in mature fields, as the erection of additional dedicated polymer treatment facilities can seriously harm the project's business case. These existing facilities often exhibit a reliable design, but do not necessarily fulfill the requirements of treating back-produced polymer. An optimization of installed facilities based on prior assessment of limitations is a way to upgrade facilities with regard to future EOR operations. Since its start-up in 2015, the main PWT plant comprised three separation stages: corrugated plate interceptors (CPIs), dissolved gas flotations (DGFs) and nutshell filters (NSFs). The plant processes up to 1,200 m3/h of conventional produced water at the Matzen field in Austria. Additionally, in 2009 a polymer injection pilot was initiated, with continuous polymer injection started in 2012, and now produces a segregated water stream containing back-produced polymer. Prior field tests with a pilot scale water treatment plant indicated operational issues with the existing set-up of facilities and the flotation chemicals used, with increasing polymer concentrations. At the end of 2018, severe injectivity issues were observed at injectors which were supplied with commingled conventional and polymer containing produced water. These were caused by a chemical interaction between the partially hydrolyzed polyacrylamide (HPAM) and alumina-based water clarifiers, which were applied in the dissolved gas flotation, finally leading to a loss of production. Therefore, a strict segregation of polymer and conventional streams at the common well network has been developed and established, where the separated streams could be injected into different parts of the injection system without any issues. This experience pointed out the future risks and hurdles of an economic cEOR full field roll-out where up to 200 ppm back-produced polymer at all surface treatment facilities is expected. Several studies were performed to identify alternative technologies able to treat polymer containing water. A business case driven option was to initiate an optimization program to develop smart upgrades and ensure maximum use of the existing PWT facilities. The main task was to substitute or stop the current poly-aluminum chloride-based coagulant in the DGF with a dosage of 40 to 60 ppm due to its unfavorable interactions with the back-produced HPAM. A technology assessment, comprehensive measures and economic retrofits of the installed gas dissolving units, the circulation cycle and bubble injection points resulted in a 200% higher flotation bubble bed density. Thanks to these improvements, the dosage of water clarifiers could be stopped, accomplishing similar or even better PWT performance values. In addition to the operational savings achieved, the existing treatment plant can now be used to treat cEOR fluids, as first tests with up to 59 ppm of back-produced polymer proved. Considering this new opportunity, a customized and economic modular cEOR debottlenecking concept was developed.
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智能升级,最大限度地利用现有采出水处理设施的CEOR
最大限度地利用现有的地面采出水处理(PWT)设施是成熟油田实现经济的化学提高采收率(cEOR)的先决条件,因为安装额外的专用聚合物处理设施可能会严重损害项目的商业价值。这些现有设施通常具有可靠的设计,但不一定能满足处理回产聚合物的要求。在预先评估限制的基础上对已安装的设施进行优化,是一种针对未来EOR操作升级设施的方法。自2015年启动以来,主要的PWT工厂包括三个分离阶段:波纹板截流器(cpi)、溶解气体浮选(dgf)和果壳过滤器(nsf)。该工厂在奥地利Matzen油田处理高达1200立方米/小时的常规采出水。此外,2009年开始了聚合物注入试验,2012年开始连续注入聚合物,现在产生了含有回产聚合物的分离水流。先前对一个中试规模的水处理厂进行的实地测试表明,随着聚合物浓度的增加,现有设施的设置和所使用的浮选化学品存在操作问题。2018年底,在注入常规和含聚合物采出水的注入器中发现了严重的注入性问题。这是由于部分水解的聚丙烯酰胺(HPAM)与用于溶气浮选的氧化铝基净水剂之间的化学相互作用造成的,最终导致产量损失。因此,在普通井网络中,聚合物和常规流体的严格分离已经开发并建立起来,分离的流体可以被注入到注入系统的不同部分而不会出现任何问题。这一经验表明,在所有地面处理设施中,回产聚合物的含量可达200ppm,在全面推广cEOR的过程中,未来存在的风险和障碍。进行了几项研究,以确定能够处理含水聚合物的替代技术。一个商业案例驱动的选择是启动一个优化程序来开发智能升级,并确保最大限度地利用现有的PWT设施。主要任务是替代或停止目前DGF中用量为40 - 60ppm的聚氯化铝基混凝剂,因为它与回产的HPAM有不利的相互作用。对已安装的气溶装置、循环周期和注泡点进行了技术评价、综合措施和经济改造,使浮选气泡床密度提高了200%。由于这些改进,净水剂的用量可以停止,实现类似甚至更好的PWT性能值。除了节省操作成本外,现有的处理厂现在可以用于处理cEOR流体,第一次测试表明,回产聚合物的含量高达59 ppm。考虑到这一新的机遇,开发了一种定制的、经济的模块化cEOR去瓶颈概念。
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