{"title":"引水隧洞 K14+716~K14+758 变形洞段“戴帽混凝土”施 工的研究及应用","authors":"刘 刚","doi":"10.26789/szgc.v7i5.1112","DOIUrl":null,"url":null,"abstract":"水电站引水隧洞地质条件极其复杂的情况下,多处存在渗水、股状涌水现象,常规施工无法顺利实现的,结合现场实际情况,最终采用“逆作法”的施工方法,顺利按期实现了变形洞段、塌方洞段的施工,对类似工程施工具有较好的借鉴 作用。","PeriodicalId":58331,"journal":{"name":"城乡建设","volume":"10 1","pages":""},"PeriodicalIF":0.0000,"publicationDate":"2022-05-16","publicationTypes":"Journal Article","fieldsOfStudy":null,"isOpenAccess":false,"openAccessPdf":"","citationCount":"0","resultStr":null,"platform":"Semanticscholar","paperid":null,"PeriodicalName":"城乡建设","FirstCategoryId":"1087","ListUrlMain":"https://doi.org/10.26789/szgc.v7i5.1112","RegionNum":0,"RegionCategory":null,"ArticlePicture":[],"TitleCN":null,"AbstractTextCN":null,"PMCID":null,"EPubDate":"","PubModel":"","JCR":"","JCRName":"","Score":null,"Total":0}
引用次数: 0
引水隧洞 K14+716~K14+758 变形洞段“戴帽混凝土”施 工的研究及应用
水电站引水隧洞地质条件极其复杂的情况下,多处存在渗水、股状涌水现象,常规施工无法顺利实现的,结合现场实际情况,最终采用“逆作法”的施工方法,顺利按期实现了变形洞段、塌方洞段的施工,对类似工程施工具有较好的借鉴 作用。
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