{"title":"Underground Bacteria Generates H 2 S and Trips Control Panels","authors":"T. Subramanian, Khaled M. Adel, I. A. Awadhi","doi":"10.2118/177798-PA","DOIUrl":null,"url":null,"abstract":"The building, having approximate dimensions of 42-m length, 9.7-m width, and 5.2-m height, is constructed of reinforced concrete walls and roof, and is designed to be blast resistant. There are four rooms in the building: the control room, which houses the instrumentation panels; the uninterrupted-power-supply (UPS) room, which houses the UPS equipment; the battery room; and the HVAC room. The panels in the equipment room are mounted on raised access flooring (false floor), having space for cables running underneath. The plan view of the building is shown in Fig. 1. The panels in this building tripped frequently, leading to unplanned plant outages, and thereby posing a risk to overall plant operations and integrity. It was observed that tripping of panels was mainly caused by failure of the electronic cards in the panels. Multiple cards had to be replaced, depending on the failure, and the rate of replacement was once in an approximately 1-month interval. Visual inspection of the cards did not indicate any defect. Site survey observations indicated a mild odor of H2S prevalent in the vicinity of the building and in areas under the false floor, discoloration of soil surrounding the building, high groundwater levels, and damages to building cable-entry sealants. To investigate the root cause and provide remedial measures, a technical study involving several testing techniques was carried out and the root cause was identified. Remedial measures were proposed to overcome the issue and were implemented at site. This paper presents the tests carried out during the study, the test results, and the recommended remedial measures and their implementation and effectiveness, which enabled mitigation of the failure of the control panels.","PeriodicalId":19446,"journal":{"name":"Oil and gas facilities","volume":"54 1","pages":""},"PeriodicalIF":0.0000,"publicationDate":"2016-06-01","publicationTypes":"Journal Article","fieldsOfStudy":null,"isOpenAccess":false,"openAccessPdf":"","citationCount":"0","resultStr":null,"platform":"Semanticscholar","paperid":null,"PeriodicalName":"Oil and gas facilities","FirstCategoryId":"1085","ListUrlMain":"https://doi.org/10.2118/177798-PA","RegionNum":0,"RegionCategory":null,"ArticlePicture":[],"TitleCN":null,"AbstractTextCN":null,"PMCID":null,"EPubDate":"","PubModel":"","JCR":"","JCRName":"","Score":null,"Total":0}
引用次数: 0
Abstract
The building, having approximate dimensions of 42-m length, 9.7-m width, and 5.2-m height, is constructed of reinforced concrete walls and roof, and is designed to be blast resistant. There are four rooms in the building: the control room, which houses the instrumentation panels; the uninterrupted-power-supply (UPS) room, which houses the UPS equipment; the battery room; and the HVAC room. The panels in the equipment room are mounted on raised access flooring (false floor), having space for cables running underneath. The plan view of the building is shown in Fig. 1. The panels in this building tripped frequently, leading to unplanned plant outages, and thereby posing a risk to overall plant operations and integrity. It was observed that tripping of panels was mainly caused by failure of the electronic cards in the panels. Multiple cards had to be replaced, depending on the failure, and the rate of replacement was once in an approximately 1-month interval. Visual inspection of the cards did not indicate any defect. Site survey observations indicated a mild odor of H2S prevalent in the vicinity of the building and in areas under the false floor, discoloration of soil surrounding the building, high groundwater levels, and damages to building cable-entry sealants. To investigate the root cause and provide remedial measures, a technical study involving several testing techniques was carried out and the root cause was identified. Remedial measures were proposed to overcome the issue and were implemented at site. This paper presents the tests carried out during the study, the test results, and the recommended remedial measures and their implementation and effectiveness, which enabled mitigation of the failure of the control panels.
该建筑的尺寸约为42米长,9.7米宽,5.2米高,由钢筋混凝土墙和屋顶构成,并设计为防爆。大楼里有四个房间:控制室,里面放着仪表面板;UPS (uninterrupted power supply)机房,存放UPS设备;蓄电池室;和暖通空调房间。机房内的面板安装在架空通道地板(假地板)上,下方有空间供电缆运行。建筑平面视图如图1所示。该建筑的面板经常跳闸,导致工厂计划外停机,从而对整个工厂的运营和完整性构成风险。据观察,面板跳闸主要是由面板中的电子卡故障引起的。根据故障情况,必须更换多张卡片,更换频率大约为1个月一次。对卡片的目视检查没有发现任何缺陷。现场调查结果显示,建筑物附近和假地板下区域普遍存在轻微的H2S气味,建筑物周围土壤变色,地下水位高,建筑物电缆入口密封剂损坏。为了调查根本原因并提供补救措施,进行了一项涉及几种测试技术的技术研究,并确定了根本原因。为了克服这个问题,我们提出了补救措施,并在现场实施。本文介绍了在研究期间进行的测试、测试结果、建议的补救措施及其实施和有效性,从而减轻了控制面板的故障。