Method Of Valve Preventive Maintenance Via Additional Overview On Pos For Decreasing Failure Risk At Starting And Change Over Fuel Gas To Fuel Oil In Block 1 And 2 Gas Turbine GT13E2 PT. PJB UP Muara Tawar

M. AlqaNury, S. Sugianto, S. N. Ihsan, K. Gunawan, T. R. Biyanto
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Abstract

Block 1 and 2 Combined Cycle Power Plant (CCPP) Muara Tawar have 5 units gas turbine can be operated by using fuel gas. Due to limitation of fuel gas from gas company. Several gas turbine are operated using High Speed Diesel fuel (HSD) to fulfil load demand. The equipment that used for fuel gas system must have high realibility to serve in dual fuel system neither operated using fuel oil or gas without unit trip. In actual, there are several disturbances occur during change over from gas to oil, even when the plant operated using fuel oil. From the data of failure causes, one of the failure causes is valve failure. By considering the availbility of plant, in term of possibility to modify instrumentation and control system, gas turbine 1.3 was choosen as object of the study. Additional indicator in HMI can be described as follows additional pressure switch attribute at EDS-P3 using symbol K, upload program to EPROM at card 70BK06 as communication card, and the cycle time less than 1 second in both valve open or close. It indicate valve system under good condition or no maintenance action is required. Valve maintenance at gas turbine ALSTOM 13E2 in Block 1 and 2 CCPP Muara Tawar can be done by additional indicator of pressure switch and aux relay contact as feedback signal on POS 30. Therefore, no disturbances in valve system and gas turbine performance increases.
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通过对GT13E2第1和第2块燃气轮机启动和燃气转燃油故障风险的额外概述的阀门预防性维护方法
Muara Tawar第一座和第二座联合循环发电厂(CCPP)有5台燃气轮机,可以使用燃气来运行。由于燃气公司的燃气限制。一些燃气轮机使用高速柴油(HSD)来满足负荷需求。用于燃气系统的设备必须具有高的可靠性,才能在双燃料系统中运行,既不使用燃油,也不使用燃气。实际上,在从天然气到石油的转换过程中,甚至当工厂使用燃油运行时,也会发生一些干扰。从失效原因的数据来看,其中一个失效原因是阀门失效。考虑到电厂的可用性,考虑到仪表和控制系统的修改可能性,选择燃气轮机1.3作为研究对象。HMI中的附加指示器描述如下:EDS-P3附加压力开关属性,使用符号K,将程序上传到70BK06卡的EPROM作为通信卡,阀门开启或关闭的周期时间小于1秒。表示阀门系统状态良好或不需要进行维护。Muara Tawar地块1和2 CCPP ALSTOM 13E2燃气轮机的阀门维护可以通过附加压力开关指示器和辅助继电器触点作为POS 30上的反馈信号来完成。因此,阀系统无扰动,燃气轮机性能提高。
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