In-Situ and Laboratory Investigation on Leaching and Effects of Early Curing of Shotcrete

IF 0.7 Q4 CONSTRUCTION & BUILDING TECHNOLOGY Nordic Concrete Research Pub Date : 2019-12-01 DOI:10.2478/ncr-2019-0014
A. Sjölander, A. Ansell
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引用次数: 1

Abstract

Abstract During the construction of a rock tunnel in Stockholm, several sections with leaching shotcrete (sprayed concrete) were found one year after the spraying was completed. An investigation was therefore conducted, and its results are presented in this paper. The amount of leaching after such a short time indicated that a one-sided water pressure existed in combination with a permeable shotcrete. The reason for the water pressure was likely a partly unsuccessful grouting that created sections with leaking water. The permeable shotcrete could be a combined result of insufficient curing and the use of accelerators, and the effect of in-situ curing was therefore investigated. A total of six slabs were sprayed and cured under different conditions in the tunnel. Test results according to standards indicated that curing has no significant effect on the development of mechanical strength or water penetration through the shotcrete. However, this is believed to be a result of the test method rather than the non-existing effect of curing. Lastly, some modifications to the test standard were proposed for future studies of in-situ curing.
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喷射混凝土浸出及早期养护效果的现场与室内研究
摘要在斯德哥尔摩某岩质隧道施工过程中,在施工完成一年后,发现多段喷淋混凝土(喷淋混凝土)渗漏。因此,进行了一项调查,并在本文中介绍了其结果。如此短时间后的浸出量表明,在透水喷射混凝土的作用下,存在单边水压。造成水压的原因很可能是部分不成功的灌浆造成了漏水的部分。透水喷射混凝土可能是养护不足和使用促进剂共同作用的结果,因此研究了原位养护对透水喷射混凝土的影响。在隧道内不同条件下,共对6块板进行了喷涂和固化。按标准进行的试验结果表明,养护对喷射混凝土的机械强度发展和水渗透性无显著影响。然而,这被认为是测试方法的结果,而不是固化不存在的影响。最后,对试验标准进行了修改,为今后的原位养护研究提供参考。
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来源期刊
Nordic Concrete Research
Nordic Concrete Research CONSTRUCTION & BUILDING TECHNOLOGY-
自引率
20.00%
发文量
8
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