{"title":"黄铜管接头的应力裂纹","authors":"Karin Kuhn","doi":"10.31399/asm.fach.process.c9001190","DOIUrl":null,"url":null,"abstract":"\n Brass pipe couplings submitted for examination were deep-drawn from disks then annealed and subsequently cold threaded. Chemical analysis confirmed that the specified alloy Ms 63 was used for fabrication. Some of the pipe already showed fine cracks prior to their installation. In most cases however the cracks were detected after a certain period of operation. The intercrystalline course of the cracks indicated stress-cracking as it often appears in brass after heavier cold deformation. The splitting of the couplings could have been avoided by a tempering heat treatment at temperatures between 230 and 300 deg C after rolling the threads. This procedure would have reduced the internal stresses while maintaining strengthening gained by the cold deformation.","PeriodicalId":294593,"journal":{"name":"ASM Failure Analysis Case Histories: Processing Errors and Defects","volume":"18 1","pages":"0"},"PeriodicalIF":0.0000,"publicationDate":"2019-06-01","publicationTypes":"Journal Article","fieldsOfStudy":null,"isOpenAccess":false,"openAccessPdf":"","citationCount":"0","resultStr":"{\"title\":\"Stress Cracks in Brass Pipe Couplings\",\"authors\":\"Karin Kuhn\",\"doi\":\"10.31399/asm.fach.process.c9001190\",\"DOIUrl\":null,\"url\":null,\"abstract\":\"\\n Brass pipe couplings submitted for examination were deep-drawn from disks then annealed and subsequently cold threaded. Chemical analysis confirmed that the specified alloy Ms 63 was used for fabrication. Some of the pipe already showed fine cracks prior to their installation. In most cases however the cracks were detected after a certain period of operation. The intercrystalline course of the cracks indicated stress-cracking as it often appears in brass after heavier cold deformation. The splitting of the couplings could have been avoided by a tempering heat treatment at temperatures between 230 and 300 deg C after rolling the threads. This procedure would have reduced the internal stresses while maintaining strengthening gained by the cold deformation.\",\"PeriodicalId\":294593,\"journal\":{\"name\":\"ASM Failure Analysis Case Histories: Processing Errors and Defects\",\"volume\":\"18 1\",\"pages\":\"0\"},\"PeriodicalIF\":0.0000,\"publicationDate\":\"2019-06-01\",\"publicationTypes\":\"Journal Article\",\"fieldsOfStudy\":null,\"isOpenAccess\":false,\"openAccessPdf\":\"\",\"citationCount\":\"0\",\"resultStr\":null,\"platform\":\"Semanticscholar\",\"paperid\":null,\"PeriodicalName\":\"ASM Failure Analysis Case Histories: Processing Errors and Defects\",\"FirstCategoryId\":\"1085\",\"ListUrlMain\":\"https://doi.org/10.31399/asm.fach.process.c9001190\",\"RegionNum\":0,\"RegionCategory\":null,\"ArticlePicture\":[],\"TitleCN\":null,\"AbstractTextCN\":null,\"PMCID\":null,\"EPubDate\":\"\",\"PubModel\":\"\",\"JCR\":\"\",\"JCRName\":\"\",\"Score\":null,\"Total\":0}","platform":"Semanticscholar","paperid":null,"PeriodicalName":"ASM Failure Analysis Case Histories: Processing Errors and Defects","FirstCategoryId":"1085","ListUrlMain":"https://doi.org/10.31399/asm.fach.process.c9001190","RegionNum":0,"RegionCategory":null,"ArticlePicture":[],"TitleCN":null,"AbstractTextCN":null,"PMCID":null,"EPubDate":"","PubModel":"","JCR":"","JCRName":"","Score":null,"Total":0}
引用次数: 0

摘要

黄铜管接头提交检查深拉盘,然后退火,随后冷螺纹。化学分析证实,制造过程中使用了指定的合金ms63。一些管道在安装之前就已经出现了细小的裂缝。然而,在大多数情况下,裂纹是在运行一段时间后检测到的。裂纹的晶间过程表明黄铜在较大的冷变形后经常出现应力开裂。在轧制螺纹后,在230至300摄氏度的温度下进行回火热处理,可以避免联轴器的分裂。这种方法可以降低内应力,同时保持冷变形所获得的强化。
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Stress Cracks in Brass Pipe Couplings
Brass pipe couplings submitted for examination were deep-drawn from disks then annealed and subsequently cold threaded. Chemical analysis confirmed that the specified alloy Ms 63 was used for fabrication. Some of the pipe already showed fine cracks prior to their installation. In most cases however the cracks were detected after a certain period of operation. The intercrystalline course of the cracks indicated stress-cracking as it often appears in brass after heavier cold deformation. The splitting of the couplings could have been avoided by a tempering heat treatment at temperatures between 230 and 300 deg C after rolling the threads. This procedure would have reduced the internal stresses while maintaining strengthening gained by the cold deformation.
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