某轻质油开发井下乳化液的识别与破乳剂注入增产

Huu Huy Vu, Manisa Rangponsumrit, N. Hoang, Duy Hung Nguyen, Hai Nam Tran, Ngoc Nguyen Phi, Tony Roche, Viet Long Dang, Minh Dung Tran
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引用次数: 0

摘要

TGT油田位于越南近海,水深45米,位于Vung Tau东南约100公里处。该油田于2011年开始生产,目前日产量约为1.3万桶。产出的原油API为38-40度,在油藏条件下粘度为0.45 cP,属于轻质油。该油田由三个井口平台组成,拥有近40口生产井,均为气举井。根据实测井底流动压力(BHFP)显著高于计算值和地面井液样中观察到的乳化液两项指标,诊断TGT井生产油管中存在乳化液,乳化液在井下环境中很少出现,在周边油田也未见报道。在完成化学剂选择的实验室测试后,于2020年初进行了现场试验,通过化学剂注入管线或与举升气一起将破乳剂注入选定井的生产油管中。成功的现场试验结果表明,这些井的BHFP明显降低,产量比8口测试井提高了约13%。由于与其他IOR方法相比,该方法成本低,经济效益显著,因此长期井下破乳剂注入已被应用于其他井,以提高油田产量。与稠油开发不同,轻油油田的井下乳化液和破乳技术缺乏相关文献。本文介绍了该技术在轻质油油田的应用实例,包括生产油管中存在乳化液问题的油井的识别、选择破乳剂的实验室测试、化学剂部署的挑战以及现场试验结果。
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Identification of Downhole Emulsion in a Light Oil Development and Demulsifier Injection for Increasing Production
TGT field is located offshore Vietnam, at a water depth of 45m and approximately 100km Southeast of Vung Tau. The field started production in 2011 and is currently producing about 13k bopd. The produced crude is 38-40 deg. API with viscosity of 0.45 cP at reservoir conditions and classified as light oil. The field consists of three wellhead platforms with nearly 40 production wells, all being gas lifted. Emulsion, which is rarely encountered in downhole environment and not reported in the surrounding oil fields, was diagnosed to be present in production tubing of TGT wells by two indications: measured bottom-hole flowing pressure (BHFP) remarkably higher than calculated value, and emulsion observed on surface well fluid samples. Upon completion of the laboratory testing for chemical selection, in early 2020 a field trial was carried out by injecting demulsifier into the production tubing of selected wells via the chemical injection line or together with lift gas. A successful field trial resulted in a clear reduction of BHFP of the wells along with a production increase by approximately 13% from 8 tested wells. Due to the low-cost of the application and major economic gain compared to other IOR methods, long-term downhole demulsifier injection has been applied in additional wells for increasing the field production. Unlike for heavy oil developments, there is a lack of publications on downhole emulsion and demulsification for light oil fields. This paper describes a case study for application in a light oil field, covering identification of the wells having an emulsion issue in the production tubing, laboratory testing for selecting demulsifier, challenges in chemical deployment and the field trial results.
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