先进钻铤连接失效模式及根本原因分析

IF 1.3 4区 工程技术 Q3 ENGINEERING, PETROLEUM SPE Drilling & Completion Pub Date : 2021-09-01 DOI:10.2118/204048-pa
M. Du, Ke Li, F. Song, Haoming Li, David L. Smith, W. Blackman
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引用次数: 1

摘要

开发了先进的钻铤接头,其疲劳寿命比相应的替代接头延长了10倍。在北美已经运行了4000多个高级连接。尽管这些连接在操作中显示出了显著的抗疲劳强度改善,但仍发生了一些故障。检索并分析了多个失效连接样本的失效模式和根本原因。在失效分析中,审查了制造数据,以确定设计规范和制造部件之间可能存在的差异。对现场运行数据进行了分析,以了解连接的加载历史。还对井下流体特性进行了分析,以确定它们对接箍性能的可能影响。对井底钻具组合(BHAs)进行了数值分析,以确定载荷分布。失效连接试样在冶金实验室进行物理处理和检验。通过数值与试验相结合的分析,得出了其破坏模式及根本原因。发现这些连接的主要失效模式是疲劳。疲劳失效的根本原因可分为两类:制造原因和操作原因。在制造失效的原因中,冷轧不正确是主要原因。与操作相关的故障主要是由过载引起的。通过故障模式和根本原因分析,先进钻铤连接的制造和操作相关风险相应降低。因此,它大大提高了高级连接的质量保证。
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Failure Modes and Root-Cause Analyses of Advanced Drill-Collar Connections
Advanced drill-collar connections have been developed with 10 times extended fatigue life compared with the corresponding replaced connections. More than 4,000 advanced connections have been run in North America. Although these connections have demonstrated substantial fatigue-strength improvement in operation, some failures have occurred. Multiple failed connection samples have been retrieved and analyzed for their failure modes and the root causes. In the failure analyses, manufacturing data were reviewed to identify any possible discrepancies between design specifications and manufactured components. The field run data were analyzed for the loading histories of the connections. The downhole fluid properties were also reviewed to identify their possible effects on the connection performances. The bottomhole assemblies (BHAs) were numerically analyzed to determine the loading distributions. The failed connection samples were physically processed and inspected in a metallurgical laboratory. Based on the combined numerical and testing analyses, the conclusions on the failure modes and the root causes were drawn. It was found that the primary failure mode for these connections was fatigue. The root causes for the fatigue failures can be divided into two categories: manufacturing causes and operational causes. Among the manufacturing failure causes, incorrect cold rolling is the primary one. The operation-related failures were mainly caused by overloading. Through failure mode and root-cause analyses, the manufacturing and operational related risks for the advanced drill-collar connections were mitigated accordingly. It therefore greatly improved the quality assurance of the advanced connections.
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来源期刊
SPE Drilling & Completion
SPE Drilling & Completion 工程技术-工程:石油
CiteScore
4.20
自引率
7.10%
发文量
29
审稿时长
6-12 weeks
期刊介绍: Covers horizontal and directional drilling, drilling fluids, bit technology, sand control, perforating, cementing, well control, completions and drilling operations.
期刊最新文献
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