蒸汽驱后CO2辅助蒸汽驱技术——以新疆油田J6区块为例

Xi Changfeng, Qi Zongyao, Liu Tong, Z. Yunjun, Zhao Fang, Qingsen Yu, D. Shen, Li Xiuluan
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引用次数: 1

摘要

J6区块注汽27年,目前处于蒸汽驱后期,采收率约为50%,含水率在95%以上。特别是目前的汽油比约为12 m3 /t,已达到经济极限,开发效果不佳。蒸汽驱后4口井的岩心显示,在25 ~ 30m的产层中,只有顶部2 ~ 3m有蒸汽室,为主蒸汽通道,残余油饱和度约为20%,其余22 ~ 27m产层为热水驱替,含油饱和度为40 ~ 55%。三维物理模拟结果表明,常规蒸汽驱全段射孔从储层顶部迅速突破,汽油比从5 m3 /t迅速上升到10 m3 /t。蒸汽突破时采收率仅为20.1%,此后长期处于高汽油比阶段。在CO2辅助蒸汽驱过程中,将整口射孔采油井改为低半射孔井,采收率由20.1%提高到81.1%,汽油比为3.3m3 /t。CO2辅助蒸汽驱阶段有三个特点:一是蒸汽- CO2辅助重力泄油模式,蒸汽室从顶部2-3cm扩展到总20cm油层;其次,有一种稳定的乳化液泡沫油,其含水率为60-70%,CO2液比约为5:1 Sm3/t, CO2是一种分散的气泡,所以它的溶解性CO2液比远远大于2:1 Sm3/t。第三,CO2降低了覆盖层的热损失,保持了地层压力。计算表明,在顶层可使热损失降低10%以上。建立了9口井模式(49口井)的中试,采收率可达75%,汽油比可达2 m3 /t,乐观预测生产效果良好。
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CO2 Assisted Steam Flooding Technology after Steam Flooding - A Case Study in Block J6 of Xinjiang Oilfield
Currently Block J6 is in the later stage of steam flooding after 27 years’ steam injection, its recovery factor is about 50%, and the water cut is more than 95%. Particularly, the present steam oil ratio is about 12 m3(CWE)/t which has reached the economic limit and is in ineffective development. Cores from four post steam flooding drilling wells show that only top 2-3m of the total 25-30m pay zone has a steam chamber which is the main steam channel and its residual oil saturation is about 20%, the other 22-27m pay zone is displaced by hot water and its oil saturation is 40-55%. A 3D physical simulation show the conventional steam flooding with full interval perforation quickly broke through from the top of reservoir, and the steam oil ratio rose rapidly from 5 m3(CWE)/t to 10 m3(CWE)/t. The recovery factor was only 20.1% at the time of steam breakthrough, and then it was in the phase of high steam oil ratio for a long time. During CO2 assisted steam flooding the whole perforated producer is switched into a low half perforated well, and the recovery factor increases from 20.1% to 81.1%, the steam oil ratio is 3.3m3(CWE)/t. There are three characteristics in CO2 assisted steam flooding stage, firstly there is a steam and CO2 assisted gravity drainage mode, steam chamber expands from the top 2-3cm to the total 20cm oil layer. Secondly, there is a stable emulsion foam oil, its water cut is 60-70%, CO2 liquid ratio is about 5:1 Sm3/t, CO2 is a kind of dispersed bubble so it is much more than the dissolved CO2 liquid ratio 2:1 Sm3/t. Thirdly, CO2 lows the heatloss to overburden and keeps the formation pressure. The calculation shows that the heat loss can be reduced by more than 10% in the top layer. A pilot test including 9 well patterns(49 wells) has been established, and its recovery factor will be up to 75%, and the steam oil ratio will up to 2 m3(CWE)/t, a good production performance is predicted optimistically.
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