用统计过程控制的方法克服600毫升瓶装瓶装的缺陷

Mahros Darsin, M. Asrofi, Joni Anggianto, Soesatijono Soesatijono
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引用次数: 0

摘要

本研究的目的是找出PT TIB 11月生产600 ml瓶装水过程中存在的缺陷类型,并对问题的解决进行一些尝试。采用统计过程控制的p图。2019年9月的控制图显示,部分数据超出了最终控制极限(UCL)。缺陷分为三种:发白、变形和断裂。Pareto图显示上述缺陷分别为59.7%,26.36%和15.07%。利用鱼骨图找到了缺陷产生的根本原因。首先,工作场所温度不稳定,在吹制之前扰乱了预成型的熔化过程,因此导致瓶子变白。其次,在加工过程中经常关闭加热器,造成偏差。加热器频繁关闭是由于软管的裂纹损坏和过期造成的。提出了一些建议,其中之一是用新的软管更换软管。2019年10月的新控制图显示,更换软管后的所有数据都在限制范围内。它还将缺陷率从0.74%降低到0.55%,降低了0.19%。
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Upaya mengatasi cacat produksi botol kemasan air 600 ml dengan metode Statistical Process Control
This research aim is to find out the type of defects in production process of 600 ml bottle water at PT TIB Jember, then some attempts to resolve the problem. The p-chart of Statistical Process Control was employed. The control chart in September 2019 shown that some data beyond the ultimate control limit (UCL). The defects were categorized into three: whitening, deviate form, and broken. The Pareto chart revealed that the aforementioned defects were 59.7%, 26.36% and 15.07% respectively. By using the fishbone diagram some root cause of the defects were found. First, the unstable workplace temperature which disturbs the preform melting process prior to blowing, therefore causing whitening the bottle. Second, the heater which is often turned off while processing that caused deviate form. The frequently turned off the heater was caused by cracked-damage along with the hoses of overdue. Some suggestions were given, one of them was replacing the hoses by the new ones. The new control chart in October 2019 showed that all data within the limits following the replacement of the hose. It also reduced the rate of the defect by 0.19% from 0.74% to 0.55%.
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