基于Gemini表面活性剂和纳米材料的高效卸泡剂的研制与现场试验

W. Junwen, Jia Wenfeng, Zhang Ru-sheng, Cen Xueqi, W. Haibo, Niu Jun
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摘要

为解决高温、高矿化度、高浓度H2S气、凝析气等含液气井的卸载问题,研制了高效泡沫卸料剂。合成具有特殊梳状结构的Gemini阴离子表面活性剂作为发泡剂分子,采用具有一定尺寸和疏水性的改性纳米颗粒作为固体泡沫稳定剂,设计合成氟碳表面活性剂作为抗凝析组分。室内实验结果表明,在温度高达150℃、盐度高达250000 ppm、H2S浓度高达2000 ppm的条件下,泡沫卸荷剂均表现出良好的起泡和稳泡能力。当凝析气体积分数高达50%时,泡沫卸荷剂具有良好的载液能力。该泡沫卸油剂在龙凤山北201-XY井的现场试验表明,平均产气量从7256 m3/天提高到11329 m3/天,提高了56%,油管与套管平均压差从2.66 MPa下降到2.38 MPa,下降了10.5%,产液量和产气量均明显,证明泡沫卸油剂能够满足高含量凝析气田排水采气的需求。
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The Development and Field Test of High Efficient Foam Unloading Agent Based on Gemini Surfactant and Nanomaterials
The high efficient foam unloading agent was developed to solve the problem of unloading of liquid loading gas well with high gas temperature, salinity and high concentration of H2S gas and gas condensate. The Gemini anionic surfactant with special comb structure was synthesized as foaming agent molecule, the modified nanoparticles with certain size and degree of hydrophobicity was adopted as solid foam stabilizer, and the fluorocarbon surfactant was designed and synthesised as gas condensate resistance components. The indoor experiment results show that the foam unloading agent showed good foaming and foam stabilizing ability when the temperature is as high as 150°C, salinity is up to 250000 ppm and H2S concentration up to 2000 ppm. Besides, the foam unloading agent present good liquid carrying ability when the volume fraction of gas condensate is as high as 50%. The field test of this foam unloading agent in Longfengshan north 201-XY well shows that, the average gas production increased from 7256 m3/day to 11329 m3/day, increased by 56%, the average differential pressure between tubing and casing dropped from 2.66 MPa to 2.38 MPa, fell by 10.5%, both liquid yield and gas production are obvious, which prove that the foam unloading agent can meet the demand of drainage gas recovery for high content gas condensate gas field.
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