{"title":"基于实验设计的螺旋分级机运行参数优化","authors":"K. Ackah, C. Owusu, F. Amoah","doi":"10.4314/gm.v20i1.5","DOIUrl":null,"url":null,"abstract":"Abstract \nClassifying Mn Ore to improve upon the grade and the properties has become a crucial activity for the Mn industry since it increases the market value of the ore. Ghana Manganese Company (GMC) has renovated their oxide washing plant by integrating it with a spiral classifier to make a batch system operating process. Particle size of <3.35mm (Mn grade of 43-47%) obtained from the primary section of the plant served as feed to the classifier and with the plant condition (i.e. at 60 min washing time, 30 rev/min speed of spirals and feed tonnage of 6 t), Mn grade of 49% was achieved. This paper focused on the optimisation of some selected operational parameters of the classifier to obtain a Mn grade >50% using Design of Experiment (DOE). Series of test works were designed using the DOE for the classifier using the constraints of washing time (30-90 min), speed of spirals (20-40 rev/min) and feed tonnage (6-9 t). The outcome of the test work after simulation showed that all the selected parameters had a great influence on Mn grade. The spiral speed and feed tonnage correlated negatively to the Mn grade with washing time correlating positively. Operating the spiral classifier at a feed rate, spiral speed and washing time of 6 t, 25 rev/min, and 30 min, respectively, yielded Mn grade of 53%. A Confirmatory test using the established conditions gave a Mn grade of 53%, which is a 4% increment in the previous Mn grade which was 47%. The outcome of the studies is the new established operational conditions which is adhered to by the plant, producing a manganese concentrate grade ranging between 52-54%. \n \nKeywords: Design of Experiment (DOE), Spiral Classifier, Grade, Manganese","PeriodicalId":12530,"journal":{"name":"Ghana Mining Journal","volume":"7 1","pages":""},"PeriodicalIF":0.0000,"publicationDate":"2020-07-07","publicationTypes":"Journal Article","fieldsOfStudy":null,"isOpenAccess":false,"openAccessPdf":"","citationCount":"1","resultStr":"{\"title\":\"Optimisation of Operational Parameters of a Spiral Classifier Using Design of Experiment (DOE)\",\"authors\":\"K. Ackah, C. Owusu, F. Amoah\",\"doi\":\"10.4314/gm.v20i1.5\",\"DOIUrl\":null,\"url\":null,\"abstract\":\"Abstract \\nClassifying Mn Ore to improve upon the grade and the properties has become a crucial activity for the Mn industry since it increases the market value of the ore. Ghana Manganese Company (GMC) has renovated their oxide washing plant by integrating it with a spiral classifier to make a batch system operating process. Particle size of <3.35mm (Mn grade of 43-47%) obtained from the primary section of the plant served as feed to the classifier and with the plant condition (i.e. at 60 min washing time, 30 rev/min speed of spirals and feed tonnage of 6 t), Mn grade of 49% was achieved. This paper focused on the optimisation of some selected operational parameters of the classifier to obtain a Mn grade >50% using Design of Experiment (DOE). Series of test works were designed using the DOE for the classifier using the constraints of washing time (30-90 min), speed of spirals (20-40 rev/min) and feed tonnage (6-9 t). The outcome of the test work after simulation showed that all the selected parameters had a great influence on Mn grade. The spiral speed and feed tonnage correlated negatively to the Mn grade with washing time correlating positively. Operating the spiral classifier at a feed rate, spiral speed and washing time of 6 t, 25 rev/min, and 30 min, respectively, yielded Mn grade of 53%. A Confirmatory test using the established conditions gave a Mn grade of 53%, which is a 4% increment in the previous Mn grade which was 47%. The outcome of the studies is the new established operational conditions which is adhered to by the plant, producing a manganese concentrate grade ranging between 52-54%. \\n \\nKeywords: Design of Experiment (DOE), Spiral Classifier, Grade, Manganese\",\"PeriodicalId\":12530,\"journal\":{\"name\":\"Ghana Mining Journal\",\"volume\":\"7 1\",\"pages\":\"\"},\"PeriodicalIF\":0.0000,\"publicationDate\":\"2020-07-07\",\"publicationTypes\":\"Journal Article\",\"fieldsOfStudy\":null,\"isOpenAccess\":false,\"openAccessPdf\":\"\",\"citationCount\":\"1\",\"resultStr\":null,\"platform\":\"Semanticscholar\",\"paperid\":null,\"PeriodicalName\":\"Ghana Mining Journal\",\"FirstCategoryId\":\"1085\",\"ListUrlMain\":\"https://doi.org/10.4314/gm.v20i1.5\",\"RegionNum\":0,\"RegionCategory\":null,\"ArticlePicture\":[],\"TitleCN\":null,\"AbstractTextCN\":null,\"PMCID\":null,\"EPubDate\":\"\",\"PubModel\":\"\",\"JCR\":\"\",\"JCRName\":\"\",\"Score\":null,\"Total\":0}","platform":"Semanticscholar","paperid":null,"PeriodicalName":"Ghana Mining Journal","FirstCategoryId":"1085","ListUrlMain":"https://doi.org/10.4314/gm.v20i1.5","RegionNum":0,"RegionCategory":null,"ArticlePicture":[],"TitleCN":null,"AbstractTextCN":null,"PMCID":null,"EPubDate":"","PubModel":"","JCR":"","JCRName":"","Score":null,"Total":0}
Optimisation of Operational Parameters of a Spiral Classifier Using Design of Experiment (DOE)
Abstract
Classifying Mn Ore to improve upon the grade and the properties has become a crucial activity for the Mn industry since it increases the market value of the ore. Ghana Manganese Company (GMC) has renovated their oxide washing plant by integrating it with a spiral classifier to make a batch system operating process. Particle size of <3.35mm (Mn grade of 43-47%) obtained from the primary section of the plant served as feed to the classifier and with the plant condition (i.e. at 60 min washing time, 30 rev/min speed of spirals and feed tonnage of 6 t), Mn grade of 49% was achieved. This paper focused on the optimisation of some selected operational parameters of the classifier to obtain a Mn grade >50% using Design of Experiment (DOE). Series of test works were designed using the DOE for the classifier using the constraints of washing time (30-90 min), speed of spirals (20-40 rev/min) and feed tonnage (6-9 t). The outcome of the test work after simulation showed that all the selected parameters had a great influence on Mn grade. The spiral speed and feed tonnage correlated negatively to the Mn grade with washing time correlating positively. Operating the spiral classifier at a feed rate, spiral speed and washing time of 6 t, 25 rev/min, and 30 min, respectively, yielded Mn grade of 53%. A Confirmatory test using the established conditions gave a Mn grade of 53%, which is a 4% increment in the previous Mn grade which was 47%. The outcome of the studies is the new established operational conditions which is adhered to by the plant, producing a manganese concentrate grade ranging between 52-54%.
Keywords: Design of Experiment (DOE), Spiral Classifier, Grade, Manganese