Chisom Emmanuel Aralu, Daniel Eseoghene Karakitie, David Abimbola Fadare
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The designed digester was a plant capacity of 4m<sup>3</sup> with a retention time of 35 days. The existing digester was demolished and the new digester was erected in its stead. The entire plant was made of reinforced concrete. The digester was loaded with 180 kg of dung daily, with a mix ratio (dung to water) of 1:1.</p><p>A 2 m<sup>3</sup> gas bag was connected to the gas outlet for collection of the produced gas. Gas production started after the 7th day of loading the digester with substrate. The collected gas was tested for burnability. The initial burn test quenched the flame and the digester was allowed for a week without feeding. The biogas burnt with a blue flame during the second test. 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引用次数: 3
摘要
对清洁能源和可再生能源的追求已成为当前能源市场的推动力,逐步摆脱对化石燃料的完全依赖。通过厌氧消化有机废物生产沼气为能源供应、回收和废物处理提供了另一种选择。位于阿巴迪纳的伊巴丹大学奶牛场有一个消化器,由于效率低下而被废弃。多年来,沼气池已经被修改了几次,但没有产生任何沼气,因此,需要一个功能性的沼气池。在新消化器的建造中采用了改进的Gobar设计。在设计中引入了一种搅拌浆料的搅拌器。设计的消化池容量为4m3,停留时间为35天。拆除了现有的消化池,并在其上建造了新的消化池。整个工厂是用钢筋混凝土建造的。粪水混合比为1:1,粪水混合比为180 kg /天。一个2m3的气囊连接到气体出口,用于收集产生的气体。在向沼气池加载底物第7天后开始产气。收集的气体进行了可燃性测试。最初的燃烧试验熄灭了火焰,并允许沼气池一周不进料。在第二次测试中,沼气燃烧出蓝色火焰。提供了一个沼气烹饪炉,以便利用所产生的气体。
Construction of a pilot scale biogas digester at the University of Ibadan Dairy Farm, Abadina
The quest for cleaner energy sources and renewable energy has become a drive force in the current energy market, creating a gradual shift from total dependence on fossil fuel. Production of biogas through the anaerobic digestion of organic wastes provides an alternative for energy supply, recovery and waste treatment. The University of Ibadan Dairy Farm, Abadina has a digester which was abandoned due to its inefficiencies. The digester has been modified a couple of times over the years without yielding any biogas, hence, the need for a functional digester.
A modified Gobar design was adopted in the construction of a new digester. An agitator was introduced in the design for stirring of the slurry. The designed digester was a plant capacity of 4m3 with a retention time of 35 days. The existing digester was demolished and the new digester was erected in its stead. The entire plant was made of reinforced concrete. The digester was loaded with 180 kg of dung daily, with a mix ratio (dung to water) of 1:1.
A 2 m3 gas bag was connected to the gas outlet for collection of the produced gas. Gas production started after the 7th day of loading the digester with substrate. The collected gas was tested for burnability. The initial burn test quenched the flame and the digester was allowed for a week without feeding. The biogas burnt with a blue flame during the second test. A biogas cooking stove was made available to enable utilization of the produced gas.