绿色增产液用于提高致密砂岩地层的采收率:在油田范围内进行了超过4年的70多口井研究

Martin Shumway, Ryan McGonagle, Anthony Nerris, J. I. Aguiar, A. Mahmoudkhani, D. M. Jacobs
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摘要

自2013年以来,阿巴拉契亚盆地的传统石油产量一直处于下降状态。由于超过80%的油井产量低于15桶/天,人们对经济、环保的增产措施越来越感兴趣。对地层矿物学和储层流体的分析以及油井干预的历史表明,由于有机物的沉淀和润湿性的变化,许多井的地层受到了损害,这是产量下降速度超过预测的部分原因。本文介绍了一种基于生物表面活性剂的新型高效增产液的开发和性能,以及在Bradford Group上泥盆系完成的几口井的现场试验经验。这组74口井在粉砂岩和砂岩储层中完成,整个油田每年出现12口以上的井失败,这是由于管柱中有机沉积物的积聚。基于这些案例,提出了使用含有生物表面活性剂的新型流体进行批量增产处理,并在现场广泛实施。这些处理有效地去除了有机沉积物,将地层润湿性从油湿性转变为水湿性,从而实现了石油产量的持续增长。该项目显著减少了油井故障,74口井在18个月内没有发生与石蜡有关的井故障。该项目的结果表明,绿色增产液在减轻地层损害、减少有机物沉积和提高石油产量方面是一种很有前途的致密地层增产方法。
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Green Well Stimulation Fluids for Enhanced Oil Recovery from Tight Sand Formations: Field Wide 70+ Wells Study Over 4 Years
Legacy oil production from Appalachian basin has been in a decline mode since 2013. With more than 80% of wells producing less than 15 bbl/day, there is a growing interest in economically and environmentally viable options for well stimulation treatments. Analysis of formation mineralogy and reservoir fluids along with history of well interventions indicated formation damage in many wells due precipitation of organics and a change in wettability being partially responsible for production decline rates in excess of forecasts. The development and properties of a novel cost-effective biosurfactant based well-stimulation fluid are described here along lessons learned from several field trials in wells completed in the Upper Devonian Bradford Group. This group of 74 wells, completed in siltstone and sandstone reservoirs were presenting more than 12 well failures annually across the field, which was attributed to the accumulation of organic deposits in the tubulars. Based on these cases, batch stimulation treatments using a novel fluid comprising biosurfactants were proposed and implemented field wide. The treatments effectively removed organic deposits, changed formation wettability from oil to water wet and resulted in a sustained oil production increase. Well failures were significantly reduced as a result of this program and the group of 74 wells did not have a paraffin-related well failure for 18 months. Results from this program demonstrates the efficiency of the green well stimulation fluids in mitigating formation damage, reducing organics deposition and in increasing oil production as a promising method to stimulate tight formations.
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