Process simulation for crude oil stabilization by using Aspen Hysys

IF 2.6 Q3 ENERGY & FUELS Upstream Oil and Gas Technology Pub Date : 2021-09-01 DOI:10.1016/j.upstre.2021.100039
Hussein Al-Ali
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引用次数: 3

Abstract

Recently, a light oil from different formations is added to the existing crude oil stabilization plant to associate the production of crude which unfortunately not enough to release off all light components and as a results the true vapor pressure (TVP) exceeds the desired specification of 82737.1 Pa/12 psia for the exported oil. The Simulation results were comparable with industrial data to give a good match between the Aspen Hysys results and the industrial analysis. The existing plant operates in three stages of gas/liquid separators where it is reported that changing production conditions, such as inlet temperature, dry fluid flow rate, water flow rate and the temperature of the outlet fluid from Fired Heater, do not make the value of TVP within the permissible limits of (68947.6–82737.1) Pa / (10–12) psia. The current work studied the effect of adding a fourth vessel on the production specifications, where it shows a successful results on decreasing the TVP. It was found that, the live crude was successfully stabilized to a TVP of less than 12 psia / 82737.1 Pa when the feed dry fluid flow rate (26.4–105.6) kbd and the minimum base sediment and water cut in the feed stream is 4 Vol%. It is also found that, the temperature of fluid has a significant impact on the crude oil specifications where the inlet fluid temperature should be in range of (43–51.5) ⁰C and the differential temperature across the Fired Heater in range of (16–24) ⁰C with feed temperature range (40–55) ⁰C.

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基于Aspen Hysys的原油稳定过程模拟
最近,一种来自不同地层的轻质油被添加到现有的原油稳定装置中,以结合原油的生产,不幸的是,原油的生产不足以释放所有轻质油,因此,出口原油的真实蒸汽压(TVP)超过了82737.1 Pa/12 psia的期望规格。仿真结果与工业数据具有可比性,使Aspen Hysys的结果与工业分析结果很好地吻合。现有工厂分三级气/液分离器运行,据报道,改变生产条件,如进口温度、干流体流速、水流流速和燃烧加热器出口流体的温度,不能使TVP值在(68947.6-82737.1)Pa / (10-12) psia的允许范围内。目前的工作是研究增加第四艘船对生产规格的影响,在降低TVP方面取得了成功的结果。结果表明,当进料干流体流量为26.4-105.6 kbd,进料流中最低底泥含水率为4 Vol%时,活性原油的TVP稳定在12 psia / 82737.1 Pa以下。研究还发现,流体温度对原油规格有重大影响,其中进口流体温度应在(43-51.5)⁰C范围内,燃烧加热器的温差应在(16-24)⁰C范围内,进料温度范围为(40-55)⁰C。
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