Successful Delivery of the First Extended Reach Well Using an Integrated Multidisciplinary Approach; A Case Study in a Mature Field, Onshore Abu Dhabi UAE
A. Shahat, Mohamed Osama Abd Elmeguid, Luis Gerardo, A. Saleh, S. Almazrouei, A. B. Sumaida, A. Mutawa, Chuma Ibeziako, Faisal Siddiqui, Shamsa Al Menhali, Fawad Zain Yousfi, Rohit V. Deshmukh, Sanjiv Kumar, Ashim Dutta, R. Reddy, M. Baslaib, Alexander Mikhaylov, Lama Atallah, M. Nasrallah, W. Fares, T. Hamdan, M. Husien
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引用次数: 0
Abstract
Drilling extended reach drilling (ERD) wells starting from the planning phase and engaging various disciplines including drilling, cementing, drilling fluids and geoscience teams. The pre-well engagement and integration between multiple disciplines are vital to define the associated drilling/geosteering challenges and accordingly optimize the drilling program to deliver a successful ERD well. These challenges are included and not limited to geological model uncertainties, differential sticking, high torque and drag, ECD limitation, friction factors and expected mud losses. An integrated and optimized plan was constructed to meet the associated challenges. The drilling engineering team optimized the bottom hole assembly (BHA) design in all sections to ensure a smooth profile using optimum drill bits designs. The BHA included LWD technologies to mitigate the geological challenges and helping in determining the casing points and geosteering operations. A new generation of intelligent fully rotating high dogleg pushthe-bit rotary steerable system was selected with matched drilling bits to geosteer the well in the thin target layer while maintaining the planned target trajectory with minimum borehole tortuosity by means of realtime drilling optimization.
Effective collaboration led to successful delivery of the first extended reach well, the geosteering objectives were achieved with 100% reservoir contact and delivered 20,000 feet targeting thin carbonate layer and overcoming the complex geology environment. The well was drilled to record depth of 32,300 feet with 29% ROP improvement in same field. ECD was always maintained below the fracture gradient along with optimal hole cleaning without cuttings buildup or tight hole while reducing the wellbore friction to ensure smooth pulling out of hole operation. Cementing operations were successfully achieved and ensured zonal isolation. Furthermore, a customized and innovative drilling fluid with free RDF Non Aqueous Fluid (NAF) and compatible lubricant were deployed along the different hole sections to reduce the expected induced losses and provide proper hole cleaning. The cementing program has been optimized for the 18 5/8", 13 3/8" and 9 5/8" casings using an innovative flexible expandable lead and tail slurries with enhanced mechanical properties to mitigate the expected losses while cementing and ensure proper isolation across all formations.
The best practice of the multidisciplinary approach along with the captured lessons learned opens the door to drill more challenging wells. in addition, it proved that proper planning and execution can shift the boundaries further and gave confidence to drill even deeper.