Investigation of 150 kV capacitor voltage transformer breakdown during capacitor bank switching

A. A. Kusuma, P. Pramana, B. S. Munir
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引用次数: 2

Abstract

This paper discuss about the investigation of 150kV capacitor voltage transformer (CVT) breakdown which is occurred simultaneously after capacitor bank disconnecting process. Analysis is performed referring to the last routine maintenance and digital fault recorder (DFR) data. Based on the analysis of both data and transient simulation analysis from the model created to represent the condition during the breakdown, it can be stated that the breakdown of 150kV CVT is due to aging of dielectric material in the CVT. Dielectric material aging of this CVT lead to the reduction of insulation overvoltage withstand in which eventually the CVT is breakdown after being hit by overvoltage stress during capacitor bank switching.
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150kv电容器电压互感器在电容器组开关过程中击穿的研究
本文对150kV电容式电压互感器在电容器组断开后同时发生击穿的情况进行了研究。根据上次例行维护和数字故障记录仪(DFR)数据进行分析。通过对数据的分析和建立的模型的暂态仿真分析,可以得出150kV无级变速器击穿是由于无级变速器内介电材料老化造成的。该无级变速器介电材料老化导致绝缘耐压降低,最终导致无级变速器在电容器组切换过程中受到过电压应力的冲击而击穿。
本文章由计算机程序翻译,如有差异,请以英文原文为准。
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