{"title":"Failure of a Turbine Spacer","authors":"","doi":"10.31399/asm.fach.power.c0046963","DOIUrl":null,"url":null,"abstract":"\n A turbine spacer made of AMS 5661 alloy (Incoloy 901; composition: Fe-43Ni-13Cr-6Mo-2.5Ti) was removed from service because of a crack in the forward side of the radial rim. The crack extended axially for a distance of 16 mm across the spacer rim; radially, it extended to a depth of 6.4 mm into the web section. Analysis (visual inspection, 5000 and 10,000x TEM fractographs, chemical analysis, and 9x metallographic examination) supported the conclusions that cracking on the forward rim of the spacer occurred in fatigue that initiated on the forward rim face and that progressed into the rim and web areas. Because there was no apparent metallurgical cause for the cracking, the problem was assigned to engineering.","PeriodicalId":107406,"journal":{"name":"ASM Failure Analysis Case Histories: Power Generating Equipment","volume":null,"pages":null},"PeriodicalIF":0.0000,"publicationDate":"2019-06-01","publicationTypes":"Journal Article","fieldsOfStudy":null,"isOpenAccess":false,"openAccessPdf":"","citationCount":"0","resultStr":null,"platform":"Semanticscholar","paperid":null,"PeriodicalName":"ASM Failure Analysis Case Histories: Power Generating Equipment","FirstCategoryId":"1085","ListUrlMain":"https://doi.org/10.31399/asm.fach.power.c0046963","RegionNum":0,"RegionCategory":null,"ArticlePicture":[],"TitleCN":null,"AbstractTextCN":null,"PMCID":null,"EPubDate":"","PubModel":"","JCR":"","JCRName":"","Score":null,"Total":0}
引用次数: 0

Abstract

A turbine spacer made of AMS 5661 alloy (Incoloy 901; composition: Fe-43Ni-13Cr-6Mo-2.5Ti) was removed from service because of a crack in the forward side of the radial rim. The crack extended axially for a distance of 16 mm across the spacer rim; radially, it extended to a depth of 6.4 mm into the web section. Analysis (visual inspection, 5000 and 10,000x TEM fractographs, chemical analysis, and 9x metallographic examination) supported the conclusions that cracking on the forward rim of the spacer occurred in fatigue that initiated on the forward rim face and that progressed into the rim and web areas. Because there was no apparent metallurgical cause for the cracking, the problem was assigned to engineering.
查看原文
分享 分享
微信好友 朋友圈 QQ好友 复制链接
本刊更多论文
涡轮垫片失效
涡轮垫片由AMS 5661合金(incoly 901;成分:Fe-43Ni-13Cr-6Mo-2.5Ti)因径向轮辋前侧出现裂纹而退出使用。裂纹沿间隔条沿轴向延伸16mm的距离;在径向上,它延伸到腹板部分6.4毫米的深度。分析(目视检查,5000倍和10000倍的TEM断口,化学分析和9倍金相检查)支持了这样的结论:垫片前缘的开裂发生在疲劳中,始于前缘表面,并向边缘和腹板区域发展。由于没有明显的冶金原因导致开裂,问题被分配给工程。
本文章由计算机程序翻译,如有差异,请以英文原文为准。
求助全文
约1分钟内获得全文 去求助
来源期刊
自引率
0.00%
发文量
0
期刊最新文献
Investigation of Intergranular Stress Corrosion Cracking in the Fuel Pool at Three Mile Island Unit 1 Intergranular Fatigue Cracking of a Stainless Steel Expansion Joint Another Turbogenerator Failure Turbine Blade Failure Dezincification of Brass Tubes in a Steam Turbine Condenser
×
引用
GB/T 7714-2015
复制
MLA
复制
APA
复制
导出至
BibTeX EndNote RefMan NoteFirst NoteExpress
×
×
提示
您的信息不完整,为了账户安全,请先补充。
现在去补充
×
提示
您因"违规操作"
具体请查看互助需知
我知道了
×
提示
现在去查看 取消
×
提示
确定
0
微信
客服QQ
Book学术公众号 扫码关注我们
反馈
×
意见反馈
请填写您的意见或建议
请填写您的手机或邮箱
已复制链接
已复制链接
快去分享给好友吧!
我知道了
×
扫码分享
扫码分享
Book学术官方微信
Book学术文献互助
Book学术文献互助群
群 号:481959085
Book学术
文献互助 智能选刊 最新文献 互助须知 联系我们:info@booksci.cn
Book学术提供免费学术资源搜索服务,方便国内外学者检索中英文文献。致力于提供最便捷和优质的服务体验。
Copyright © 2023 Book学术 All rights reserved.
ghs 京公网安备 11010802042870号 京ICP备2023020795号-1