Failure of an Oil-Line Subassembly Because of Poor Welding

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Abstract

Several elbow subassemblies comprising segments of oil-line assemblies that recycled aircraft-engine oil from pump to filter broke in service. The components of the subassemblies were made of aluminum alloy 6061-T6. Two subassemblies were returned to the laboratory to determine cause of failure. In one, the threaded boss had separated from the elbow at the weld. In the other, the failure was by fracture of the elbow near the flange. The separation of the threaded boss from the elbow was due to a poor welding procedure. Crack propagation was accelerated by fatigue caused by cyclic service stresses. The fracture of the second elbow near the flange was caused by overaging during repair welding of the boss weld. Satisfactory weld penetration was achieved by improved training of the welders plus more careful inspection. Repair welding was prohibited, to avoid recurrence of overaging from the welding heat. Additional support for the oil line was installed to reduce vibration and minimize fatigue of the elbow.
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由于焊接不良导致油管组件失效
几个弯头组件,包括将飞机发动机油从泵循环到过滤器的油管组件,在使用中发生故障。组件采用6061-T6铝合金。两个组件被送回实验室以确定故障原因。其中一件是螺纹凸台在焊接处与弯头分离。在另一种情况下,失效是由于靠近法兰的弯头断裂。螺纹凸台与弯头的分离是由于焊接工艺不好造成的。循环使用应力引起的疲劳加速了裂纹扩展。第二弯头靠近法兰处断裂是由于凸台焊缝补焊时过度老化造成的。通过改进对焊工的培训和更仔细的检查,取得了令人满意的焊深。禁止补焊,避免焊接热引起的过老化现象再次发生。为油管安装了额外的支撑,以减少振动,最大限度地减少弯头的疲劳。
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