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Helicopter Main Rotor Transmission Output Shaft Failure 直升机主旋翼传动输出轴故障
Pub Date : 2019-06-01 DOI: 10.31399/asm.fach.aero.c9001505
J. Hutchinson
A helicopter had just taken off when there was a loud bang and the engine started to overspeed. After landing and inspection, the transmission was disassembled. It was discovered that the assembly containing the output shaft to the main rotor had failed. The output shaft assembly was made up of two parts: the output shaft with an integral 10 in. diam upper disc at approximately mid-section; and a 10 in. diam lower disc. During manufacture, the lower disc was attached to the output shaft by an electron beam weld. The fracture had a single fatigue initiation site, coincident with the annular zone of remelted material on the inner surface of the disc. In the lower disc, the fracture was also 80% fatigue, but high stress, low cycle in nature and contained multiple initiation sites coincident with an electron beam weld bead. It was concluded that fatigue in the upper disc resulted from the presence of a metallurgical stress concentration caused by the electron weld beam impingement on the inner surface of the upper disc. An Airworthiness Directive was issued, and the manufacturer issued a mandatory service bulletin outlining a periodic inspection for the output shaft assembly.
一架直升机刚起飞,就听到一声巨响,发动机开始超速。着陆和检查后,变速箱被拆卸。人们发现包含输出轴到主转子的组件已经失效。输出轴总成由两部分组成:输出轴与积分10英寸。上阀瓣直径约在中段;还有一个10英寸。下阀瓣直径。在制造过程中,下圆盘通过电子束焊接连接到输出轴上。断裂有一个单一的疲劳起始点,与圆盘内表面重熔材料的环形区域一致。下盘断裂也是80%的疲劳断裂,但本质上是高应力、低周期断裂,且含有多个与电子束焊缝重合的起始点。结果表明,上盘的疲劳是由电子束撞击上盘内表面引起的冶金应力集中引起的。发布了适航指令,制造商发布了强制性服务公告,概述了输出轴总成的定期检查。
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引用次数: 0
Corrosion-Fatigue Cracking in an AMS 6415 Steel Aircraft Shaft AMS 6415钢飞机轴的腐蚀疲劳裂纹
Pub Date : 2019-06-01 DOI: 10.31399/asm.fach.aero.c0046870
A hollow, splined alloy steel aircraft shaft (machined from an AMS 6415 steel forging – approximately the same composition as 4340 steel – then quenched and tempered to a hardness of 44.5 to 49 HRC) cracked in service after more than 10,000 h of flight time. The inner surface of the hollow shaft was exposed to hydraulic oil at temperatures of 0 to 80 deg C (30 to 180 deg F). Analysis (visual inspection, 15-30x low magnification examination, 4x light fractograph, chemical analysis, hardness testing) supported the conclusions that the shaft cracked in a region subjected to severe static radial, cyclic torsional, and cyclic bending loads. Cracking originated at corrosion pits on the smoothly finished surface and propagated as multiple small corrosion-fatigue cracks from separate nuclei. The originally noncorrosive environment (hydraulic oil) became corrosive in service because of the introduction of water into the oil. Recommendations included taking additional precautions in operation and maintenance to prevent the use of oil containing any water through filling spouts or air vents. Also, polishing to remove pitting corrosion (but staying within specified dimensional tolerances) was recommended as a standard maintenance procedure for shafts with long service lives.
一个中空的花键合金钢飞机轴(由AMS 6415钢锻件加工-与4340钢的成分大致相同-然后调质至44.5至49hrc)在飞行时间超过10,000小时后在使用中破裂。空心轴的内表面暴露在温度为0至80℃(30至180°F)的液压油中。分析(目视检查,15-30倍低倍放大检查,4倍光断口检查,化学分析,硬度测试)支持轴在遭受严重的静态径向,循环扭转和循环弯曲载荷的区域破裂的结论。裂纹起源于光滑表面的腐蚀坑,并从单独的核中扩展成多个小的腐蚀疲劳裂纹。原本无腐蚀性的环境(液压油)在使用中由于水进入油中而具有腐蚀性。建议包括在操作和维护中采取额外的预防措施,以防止通过填充喷口或通风口使用含有任何水的油。此外,抛光以消除点蚀(但要保持在规定的尺寸公差范围内)被推荐为具有长使用寿命的轴的标准维护程序。
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引用次数: 0
Failure of a Steel Bomb Suspension Lug 钢炸弹吊耳失效
Pub Date : 2019-06-01 DOI: 10.31399/asm.fach.aero.c9001906
M. Pepi
Suspension lugs fabricated from AISI 4340 steel used to facilitate loading of bombs onto the underside of military aircraft could not sustain required loads during routine proof load testing. Three failed lugs underwent visual examination, chemical analysis, metallography, hardness testing, scanning electron microscopy, and energy-dispersive x-ray spectroscopy. It was determined that the failures were due to forging defects. Both forging laps and seams acted as stress concentrators when the lugs were loaded during proof testing.
由AISI 4340钢制造的悬耳用于方便将炸弹装载到军用飞机的底部,在常规的证明载荷测试中不能承受所需的载荷。三个失败的耳片进行了目视检查、化学分析、金相、硬度测试、扫描电子显微镜和能量色散x射线光谱学。经确定,这些故障是由于锻造缺陷造成的。在验证测试中,当凸耳加载时,锻造圈和接缝都起到了应力集中的作用。
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引用次数: 0
Corrosion of Aluminum Alloy 7075-T6 Wing Panel 7075-T6铝合金翼板的腐蚀
Pub Date : 2019-06-01 DOI: 10.31399/asm.fach.aero.c0006402
New aircraft wing panels extruded from 7075-T6 aluminum exhibited an unusual pattern of circular black interrupted lines, which could not be removed by scouring or light sanding. The panels, subsequent to profiling and machining, were required to be penetrated inspected, shot peened, H2SO4 anodized, and coated with MIL-C-27725 integral fuel tank coating on the rib side. Scanning electron microscopy and microprobe analysis (both conventional energy-dispersive and Auger analyzers) showed that the anodic coating was applied over an improperly cleaned and contaminated surface. The expanding corrosion product had cracked and, in some places, had flaked away the anodized coating. The corrodent had penetrated the base aluminum in the form of subsurface intergranular attack to a depth of 0.035 mm (0.0014 in.). It was recommended that a vapor degreaser be used during cleaning prior to anodizing. A hot inhibited alkaline cleaner was also recommended during cleaning prior to anodizing. The panels should be dichromate sealed after anodizing. The use of deionized water was also recommended during the dichromate sealing operation. In addition, the use of an epoxy primer prior to shipment of the panels was endorsed. Most importantly, surveillance of the anodizing process itself was emphasized.
由7075-T6铝材挤压而成的新飞机机翼面板显示出一种不寻常的圆形黑色断线图案,这种图案无法通过冲刷或光砂去除。在成型和加工之后,面板需要进行穿透检查、喷丸处理、H2SO4阳极氧化,并在肋侧涂上MIL-C-27725整体油箱涂层。扫描电子显微镜和微探针分析(包括传统的能量色散和俄歇分析仪)表明,阳极涂层被应用在不正确清洁和污染的表面上。膨胀的腐蚀产物已经破裂,在某些地方,阳极氧化涂层已经剥落。腐蚀以表面下晶间侵蚀的形式渗入基体铝,深度为0.035 mm (0.0014 in.)。建议在阳极氧化前的清洁过程中使用蒸汽脱脂剂。在阳极氧化之前的清洁过程中,也建议使用热抑制碱性清洁剂。阳极氧化后的面板应采用重铬酸盐密封。在重铬酸盐密封过程中也建议使用去离子水。此外,批准在面板装运前使用环氧底漆。最重要的是,强调了对阳极氧化过程本身的监测。
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引用次数: 0
Failure of a Carburized Steel Generator-Drive Idler Gear by Pitting Due to Decarburization and Subsurface Oxidation 碳化钢发电机驱动惰轮因脱碳和表面氧化引起的点蚀失效
Pub Date : 2019-06-01 DOI: 10.31399/asm.fach.aero.c0048257
Evidence of destructive pitting on the gear teeth (AMS 6263 steel) in the area of the pitchline was exhibited by an idler gear for the generator drive of an aircraft engine following test-stand engine testing. The case hardness was investigated to be lower than specified and it was suggested that it had resulted from surface defects. A decarburized surface layer and subsurface oxidation in the vicinity of pitting were revealed by metallographic examination of the 2% nital etched gear tooth sample. It was concluded that pitting had resulted as a combination of both the defects. The causes for the defects were reported based on previous investigation of heat treatment facilities. Oxide layer was caused by inadequate purging of air before carburization while decarburization was attributed to defects in the copper plating applied to the gear for its protection during austenitizing in an exothermic atmosphere. It was recommended that steps be taken during heat treatment to ensure neither of the two occurred.
在试验台发动机试验后,飞机发动机发电机驱动的空转齿轮显示了俯俯线区域齿轮齿(AMS 6263钢)上破坏性点蚀的证据。经调查,其硬度低于规定,认为是由于表面缺陷造成的。通过金相检验发现,2%的数字蚀刻齿轮样品在点蚀附近有脱碳的表面层和亚表面氧化。结论是,点蚀是这两种缺陷共同作用的结果。缺陷的原因是根据以前对热处理设备的调查报告的。氧化层是由于在渗碳前空气净化不足造成的,而脱碳是由于在放热气氛中用于保护齿轮的镀铜层的缺陷造成的。建议在热处理过程中采取措施,以确保两者都不发生。
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引用次数: 0
Failure by Stress-Corrosion Cracking of an Ejection Seat Swivel 弹射座椅转轴应力腐蚀开裂失效
Pub Date : 2019-06-01 DOI: 10.31399/asm.fach.aero.c0006387
A routine examination on a seat ejection system found that the catapult attachment swivel fabricated from 7075-T651 aluminum alloy plate contained cracks on opposite sides of the part. This swivel, or bath tub, does not experience extreme loads prior to activation of the catapult system. Some loads could be absorbed however, when the aircraft is subjected to G loads. Visual examination of the part revealed that cracks through the wall thickness initiated on the inner walls of the fixture. Scanning electron microscopy (SEM) and electron optical examination revealed that the cracking pattern initiated and progressed by an intergranular failure mechanism. It was concluded that failure of the catapult attachment swivel fixture occurred by SCC. It was recommended that the 7075 aluminum ejection seat fixture be supplied in the T-73 temper to minimize susceptibility to SCC.
对座椅弹射系统的例行检查发现,由7075-T651铝合金板制成的弹射附件旋转部件在部件的相对侧存在裂纹。在弹射系统启动之前,这个旋转装置或浴缸不会经历极端载荷。然而,当飞机受到G载荷时,一些载荷可以被吸收。目视检查的部分显示,裂纹通过壁厚开始在内壁的夹具。扫描电镜(SEM)和电子光学检测表明,裂纹模式是由晶间破坏机制引发和发展的。结果表明,弹射器附件旋转夹具的失效是由SCC引起的。建议采用T-73回火的7075铝制弹射座椅夹具,以尽量减少对SCC的敏感性。
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引用次数: 0
Hydrogen Embrittlement of Cadmium-Plated Alloy Steel Self-Retaining Bolts in a Throttle-Control Linkage 阀控连杆中镀镉合金钢自扣螺栓的氢脆
Pub Date : 2019-06-01 DOI: 10.31399/asm.fach.aero.c0048630
Two clevis-head self-retaining bolts used in the throttle-control linkage of a naval aircraft failed on the aircraft assembly line. Specifications required the bolts to be heat treated to a hardness of 39 to 45 HRC, followed by cleaning, cadmium electroplating, and baking to minimize hydrogen embrittlement. The bolts broke at the junction of the head and shank. The nuts were, theoretically, installed fingertight. The failure was attributed to hydrogen embrittlement that had not been satisfactorily alleviated by subsequent baking. The presence of burrs on the threads prevented assembly to finger-tightness, and the consequent wrench torquing caused the actual fractures. The very small radius of the fillet between the bolt head and the shank undoubtedly accentuated the embrittling effect of the hydrogen. To prevent reoccurrence, the cleaning and cadmium-plating procedures were stipulated to be low-hydrogen in nature, and an adequate post plating baking treatment at 205 deg C (400 deg F), in conformity with ASTM B 242, was specified. A minimum radius for the head-to-shank fillet was specified at 0.25 mm (0.010 in.). All threads were required to be free of burrs. A 10-day sustained-load test was specified for a sample quantity of bolts from each lot.
一架海军飞机的节流阀控制连接装置中使用的两个槽头自固定螺栓在飞机装配线上失效。规格要求将螺栓热处理至39至45 HRC的硬度,然后进行清洗、镀镉和烘烤,以尽量减少氢脆。螺栓在头和柄的连接处断了。从理论上讲,这些螺母安装得很紧。失败的原因是氢脆没有通过随后的烘烤得到令人满意的缓解。螺纹上毛刺的存在使装配无法达到指紧性,而随之而来的扳手扭矩导致了实际的断裂。螺栓头和螺栓柄之间的圆角半径非常小,无疑加重了氢的脆化作用。为了防止再次发生,清洗和镀镉的程序被规定为低氢性质,并在205摄氏度(400华氏度)下进行适当的镀后烘烤处理,符合ASTM B 242的规定。头柄圆角的最小半径规定为0.25毫米(0.010英寸)。所有的螺纹都要求无毛刺。对每批螺栓的样品数量进行为期10天的持续载荷试验。
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引用次数: 0
Hydrogen Embrittlement of Aircraft Components 飞机部件的氢脆
Pub Date : 2019-06-01 DOI: 10.31399/asm.fach.aero.c9001746
Jivan B. Shah
Brittle intergranular fracture, typical of a hydrogen-induced delayed failure, caused the failure of an AISI 4340 Cr-Mo-Ni landing gear beam. Corrosion resulting from protective coating damage released nascent hydrogen, which diffused into the steel under the influence of sustained tensile stresses. A second factor was a cluster of non-metallic inclusions which had ‘tributary’ cracks starting from them. Also, eyebolts broke when used to lift a light aircraft (about 7000 lb.). The bolt failure was a brittle intergranular fracture, very likely due to a hydrogen-induced delayed failure mechanism. As for the factors involved, cadmium plating, acid pickling, and steelmaking processes introduce hydrogen on part surfaces. As a second contributing factor, both bolts were 10 Rc points higher in hardness than specified (25 Rc), lessening ductility and notch toughness. A third factor was inadequate procedure, which resulted in bending moments being applied to the bolt threads.
AISI 4340 Cr-Mo-Ni起落架梁的脆性晶间断裂是典型的氢致延迟失效。由于保护涂层的破坏而产生的腐蚀释放出新生的氢,在持续拉应力的影响下扩散到钢中。第二个因素是一簇非金属夹杂物,这些夹杂物有“支流”裂缝。此外,吊起轻型飞机(约7000磅)时,螺栓也会断裂。螺栓断裂为脆性晶间断裂,很可能是由于氢诱导的延迟破坏机制。至于所涉及的因素,镀镉、酸洗和炼钢过程会在零件表面引入氢。第二个影响因素是,两个螺栓的硬度都比规定的(25 Rc)高10 Rc点,降低了延展性和缺口韧性。第三个因素是工艺不当,导致螺栓螺纹产生弯矩。
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引用次数: 0
Failures in Airplane Engine Crankshafts 飞机发动机曲轴故障
Pub Date : 2019-06-01 DOI: 10.31399/asm.fach.aero.c9001552
Jivan B. Shah
This report covers case histories of failures in fixed-wing light aeroplane and helicopter components. A crankshaft of AISI 4340 Ni-Cr-Mo alloy steel, heat treated and nitrided all over, failed in bending fatigue. The nitrided layer was ground too rapidly causing excessive heat generation which induced grinding cracks and grinding burn. Tensional stresses resulting from grinding developed in a thin surface layer. On another crankshaft, chromium plating introduced undesirable residual tensile stresses. Such plating is an unsatisfactory finish for crankshafts of aircraft engines. Aircraft engine manufacturers and aeronautical standards require magnetic particle inspection to detect grinding cracks after reconditioning. Renitriding after any grinding is needed also, regardless of the amount of undersize as it introduces beneficial residual compressive stresses.
本报告涵盖了固定翼轻型飞机和直升机部件故障的历史案例。一种AISI 4340 Ni-Cr-Mo合金钢曲轴经热处理和全氮化处理后,发生弯曲疲劳失效。氮化层磨削过快,产生过多的热量,引起磨削裂纹和磨削烧伤。由磨削产生的拉应力在薄的表面层中产生。在另一个曲轴上,镀铬引入了不良的残余拉伸应力。这样的电镀对于飞机发动机的曲轴是不理想的。飞机发动机制造商和航空标准要求磁粉检测在修复后的磨削裂纹。任何磨削后都需要再氮化,不管尺寸过小的多少,因为它会引入有益的残余压应力。
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引用次数: 0
Bending of an Aircraft-Wing Slat Track 机翼板条轨道的弯曲
Pub Date : 2019-06-01 DOI: 10.31399/asm.fach.aero.c0092142
During a routine inspection on an aircraft assembly line, an airframe attachment bolt was found to be broken. The bolt was one of 12 that attach the lower outboard longeron to the wing carry-through structure. Failure occurred on the right-hand forward bolt in this longeron splice attachment. The bolt was fabricated from PH13-8Mo stainless steel heat treated to have an ultimate tensile strength of 1517 to 1655 MPa (220 to 240 ksi). A water-soluble coolant was used in drilling the bolt hole where this fastener was inserted. Investigation (visual inspection, 265 SEM images, hardness testing, auger emission spectroscopy and secondary imaging spectroscopy, tensile testing, and chemical analysis) supported the conclusion that failure of the attachment bolt was caused by stress corrosion. The source of the corrosive media was the water-soluble coolant used in boring the bolt holes. Recommendations included inspecting for corrosion all the bolts that were installed using the water-soluble coolant at the spliced joint areas, rinsing all machined bolt holes with a noncorrosive agent, and installing new PH13-8Mo stainless steel bolts with a polysulfide wet sealant.
在一次对飞机装配线的例行检查中,发现一个机身连接螺栓坏了。这个螺栓是12个连接较低的舷外长翼和机翼穿过结构的螺栓之一。故障发生在右手前螺栓在这个较长的接头附件。螺栓由经过热处理的PH13-8Mo不锈钢制成,其极限抗拉强度为1517至1655 MPa(220至240 ksi)。在插入该紧固件的螺栓孔上钻孔时使用了一种水溶性冷却剂。调查(目视检查、265张SEM图像、硬度测试、螺旋发射光谱和二次成像光谱、拉伸测试和化学分析)支持了附件螺栓失效是由应力腐蚀引起的结论。腐蚀介质的来源是螺栓孔钻孔时使用的水溶性冷却剂。建议包括在拼接区域使用水溶性冷却剂检查所有安装的螺栓的腐蚀情况,用非腐蚀性剂冲洗所有加工螺栓孔,并使用聚硫湿密封胶安装新的PH13-8Mo不锈钢螺栓。
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引用次数: 0
期刊
ASM Failure Analysis Case Histories: Air and Spacecraft
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