PERANCANGAN DAN MODIFIKASI MOLD INSERT UNTUK MENINGKATKAN KAPASITAS PRODUKSI LIGHT GUIDE

Benny Haddli Irawan, Putri Septaningrum, Ita Wijayanti, R. Hakim, Ihsan Saputra
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Abstract

The use of plastic is often found in human life. Therefore, many manufacturing companies are competing to increase the production and quality of their plastic products. One way to increase production is to redesign a Mold base so that the Mold has a larger production capacity than before. The increase in product demand from consumers, which was initially 65,000 pcs/month to 95,000 pcs/month, is also the background for conducting this research. The purpose of this study is to redesign the soft tool using the old Mold base. The design uses Siemens UG NX 5 software. The Mold used is a two-plate Mold. The manufacture of the core cavity uses NAK 80 steel and plastic raw material in the form of Polycarbonate (PC). At the end of the study, a simulation was carried out using the Moldex 3D Flow Mold software to see the cycle time of the old and new Mold injection processes. From the results of this study, production capacity increased from 67,804 pcs/month to 118,536 pcs/month resulting in twice as many products as the old Mold design, with an increase in cycle time of 14.37% longer than the old Mold design also ensuring the quality of the product is maintained.
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设计和改造模具镶件,提高导光板生产能力
在人类生活中,塑料的使用屡见不鲜。因此,许多制造公司都在竞相提高塑料产品的产量和质量。提高产量的方法之一是重新设计模具底座,使模具的生产能力比以前更大。消费者对产品的需求从最初的 65,000 件/月增加到 95,000 件/月,这也是开展本研究的背景。本研究的目的是利用旧模具基础重新设计软工具。设计使用西门子 UG NX 5 软件。使用的模具是双板模具。芯腔的制造使用 NAK 80 钢和聚碳酸酯 (PC) 形式的塑料原料。研究结束后,使用 Moldex 3D Flow Mold 软件进行了模拟,以了解新旧模具注塑工艺的周期时间。研究结果表明,生产能力从 67 804 件/月提高到 118 536 件/月,产品数量是旧模具设计的两倍,周期时间比旧模具设计延长了 14.37%,同时还确保了产品质量。
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