Experimental analysis of acidizing in Weizhou X low permeability reservoir

Yi Zhang, Bin Zhang, Feng Wei, Hongjun Lu, Banghua Liu, Mingguang Tang, PengYu Zhu, Rui Wang, Jian Yan
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Abstract

Aiming at the problem of increased water injection pressure and poor water injection effect during the water injection operation of Weizhou X offshore low permeability oil reservoir. The cause of clogging was clarified using cast thin section experiments, water quality compatibility experiments and reservoir sensitivity experiments, and corresponding deblocking agents were configured based on the experimental results. The experimental results show that Weizhou X oilfield has strong velocity sensitivity (damage rate 85.35%) and strong salt sensitivity (damage rate 63.02%), and there is a phenomenon of water quality incompatibility. Analysis shows that the excessive velocity of the injected water causes the core particles to fall off and the water quality is incompatible with the calcium carbonate precipitation to cause pore throat blockage as the fluid migrates to the small roar, which is the main reason for the increase in water injection pressure. Based on the analysis results, the acid solution formula was optimized and determined to be: 12% HCl + 0.5% HF + 3% CH3COOH + 0.5% C6H12N4. Indoor test results show that the acid has good clay swelling prevention and reservoir modification effects, and the average reservoir modification rate is 129.21%. The plug‐removing effect is remarkable and can be promoted in similar oil fields.
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涠洲 X 低渗透储层酸化试验分析
针对涠洲 X 海上低渗透油藏注水作业中注水压力增大、注水效果不佳的问题。通过投薄片实验、水质相容性实验和油藏敏感性实验,明确了堵塞原因,并根据实验结果配置了相应的解堵剂。实验结果表明,涠洲X油田具有较强的速度敏感性(损害率85.35%)和较强的盐敏感性(损害率63.02%),存在水质不相容现象。分析表明,注水速度过快导致岩心颗粒脱落,水质不兼容导致碳酸钙沉淀,使流体向小吼迁移时造成孔喉堵塞,这是注水压力增大的主要原因。根据分析结果,对酸液配方进行了优化,确定为:12% HCl + 0.5% HF + 3% CH3COOH + 0.5% C6H12N4。室内试验结果表明,该酸具有良好的防粘土膨胀和储层改造效果,平均储层改造率为 129.21%。除塞效果显著,可在类似油田推广。
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