Failure analysis of a diesel generator connecting rod

C. Juarez , F. Rumiche , A. Rozas , J. Cuisano , P. Lean
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引用次数: 24

Abstract

This paper presents the results of a failure analysis investigation conducted in a connecting rod from a diesel engine used in the generation of electrical energy. The investigation included an extensive analysis of the con-rod material as well as the fracture zone. The investigation involved the following experimental procedures and testing techniques: visual inspection, fractography, magnetic particle inspection, chemical analysis, tensile and hardness testing, metallography, and microanalysis. The connecting rod was fabricated from an AISI/SAE 4140 low alloy steel; chemical composition, mechanical properties and microstructure were appropriate for the application. The connecting rod fractured at the body in a section close to the head; the origin of the fracture was located at the con-rod lubrication channel. The lubrication channel exhibited an area containing a tungsten based material, presumably from a machining tool, embedded in its surface as a result of a deficient manufacturing process. This area acted as nucleation site for cracks that propagate through the connecting rod section by a fatigue mechanism, reducing its section and finally producing its catastrophic failure.

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柴油发电机连杆失效分析
本文介绍了对发电用柴油机连杆进行失效分析研究的结果。调查包括对控制杆材料和断裂带的广泛分析。调查涉及以下实验程序和测试技术:目视检查,断口检查,磁粉检查,化学分析,拉伸和硬度测试,金相学和显微分析。连杆采用AISI/SAE 4140低合金钢;化学成分、力学性能和显微组织均符合应用要求。连杆在靠近头部的一段处断裂;裂缝的源头位于控制杆润滑通道。润滑通道显示出包含钨基材料的区域,可能来自加工工具,由于制造工艺缺陷而嵌入其表面。该区域作为裂纹的形核位置,裂纹通过疲劳机制在连杆截面上扩展,减小了连杆截面,最终导致连杆的灾难性破坏。
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