Donny Ridwan Prihadi, Ronggo Ridwan Prihadi, S. H. Pranolo, J. Waluyo, Firman Asto Putro
{"title":"Optimization of Condensate Transfer Pump in the Hydrocarbon Condensate Stabilization Unit of Natural Gas Liquefaction Plant – An Industrial Case","authors":"Donny Ridwan Prihadi, Ronggo Ridwan Prihadi, S. H. Pranolo, J. Waluyo, Firman Asto Putro","doi":"10.30560/ijas.v5n2p1","DOIUrl":null,"url":null,"abstract":"PT. Badak NGL is a commercial LNG producer located in Bontang, Indonesia. In recent years, the decline in LNG production of PT. Badak NGL results in a lower hydrocarbon condensate flow rate. To prevent power losses since its pump operated at below rating, a new operation scheme was proposed. This new scheme adjusts the way of pump is operated without any alteration in terms of pump characteristics. Three pumps operated intermittently for 8 hours per day at a maximum flow rate. The pump power consumption was calculated based on electric current data monitored relay panel. The results show that the pump energy saved by 60% with the absolute value of annual energy efficiency of 957.7 MWh. This study contributes to reducing the greenhouse effect by 412 tons eq CO and the annual production cost of around USD 130,000. The new scheme reliability examines by evaluating pump vibration, pump performance, hydrocarbon condensate quality, and condensate tank liquid level. The result shows that the pump’s vibration in the range of 0.21 in/sec with a steady winding temperature.","PeriodicalId":13778,"journal":{"name":"International Journal of Applied Science and Engineering","volume":"22 1","pages":""},"PeriodicalIF":0.0000,"publicationDate":"2022-11-07","publicationTypes":"Journal Article","fieldsOfStudy":null,"isOpenAccess":false,"openAccessPdf":"","citationCount":"0","resultStr":null,"platform":"Semanticscholar","paperid":null,"PeriodicalName":"International Journal of Applied Science and Engineering","FirstCategoryId":"1085","ListUrlMain":"https://doi.org/10.30560/ijas.v5n2p1","RegionNum":0,"RegionCategory":null,"ArticlePicture":[],"TitleCN":null,"AbstractTextCN":null,"PMCID":null,"EPubDate":"","PubModel":"","JCR":"","JCRName":"","Score":null,"Total":0}
引用次数: 0
Abstract
PT. Badak NGL is a commercial LNG producer located in Bontang, Indonesia. In recent years, the decline in LNG production of PT. Badak NGL results in a lower hydrocarbon condensate flow rate. To prevent power losses since its pump operated at below rating, a new operation scheme was proposed. This new scheme adjusts the way of pump is operated without any alteration in terms of pump characteristics. Three pumps operated intermittently for 8 hours per day at a maximum flow rate. The pump power consumption was calculated based on electric current data monitored relay panel. The results show that the pump energy saved by 60% with the absolute value of annual energy efficiency of 957.7 MWh. This study contributes to reducing the greenhouse effect by 412 tons eq CO and the annual production cost of around USD 130,000. The new scheme reliability examines by evaluating pump vibration, pump performance, hydrocarbon condensate quality, and condensate tank liquid level. The result shows that the pump’s vibration in the range of 0.21 in/sec with a steady winding temperature.
期刊介绍:
IJASE is a journal which publishes original articles on research and development in the fields of applied science and engineering. Topics of interest include, but are not limited to: - Applied mathematics - Biochemical engineering - Chemical engineering - Civil engineering - Computer engineering and software - Electrical/electronic engineering - Environmental engineering - Industrial engineering and ergonomics - Mechanical engineering.