Openhole Completions as Recovery Case for Drilling Across Salt and High Pressure Floaters

A. Moiseenkov, A. Hadhrami, F. Khayrutdinov, I. Azizi, Hilal Shabibi, M. Manthari, K. Melvin, Attia Ziada, M. Rashdi, Mahmood Omairi, T. Narwal
{"title":"Openhole Completions as Recovery Case for Drilling Across Salt and High Pressure Floaters","authors":"A. Moiseenkov, A. Hadhrami, F. Khayrutdinov, I. Azizi, Hilal Shabibi, M. Manthari, K. Melvin, Attia Ziada, M. Rashdi, Mahmood Omairi, T. Narwal","doi":"10.2118/197356-ms","DOIUrl":null,"url":null,"abstract":"\n Well delivery in Pre-Cambrian salt with high-pressure floaters in the South of Oman provides several challenges, including Well Control Events, losses, supercharging, salt creeping, casing collapse and a negative drilling windows if section TD is picked incorrectly. The well design does not allow for an additional casing string with redundancy to case of troublesome zones.\n To overcome this, PDO initiated a barefoot completion as an extra hole section instead of well abandonment. As a wells recovery plan in 2017, PDO initiated different potential options to complete Ara salt wells and one of visible alternative options was to complete wells as open hole \"Barefoot\" completion. A design solution developed across technical functions on the suitability of barefoot completion in the carbonate reservoirs. The method to drill and complete with 3.615\" hole as \"Barefoot\" was then expedited through detailed design as per the well delivery process. Key factors, which were considered included inflow performance and hole stability, the review of BHA design, drilling hydraulics, fluids selection and barrier considerations for barefoot completion. The operational challenges were reviewed and optimized with each implementation to drive further value.\n To date three wells recovered successfully with the new barefoot completion method. The wells completed with solids free drilling mud placed across the reservoir section and a suspension plug installed in the upper completion to facilitate rig release. During well testing operations; the suspension plug is removed, the openhole section is clean-up with coil tubing to remove filter cake with Enzyme treatment and finally the carbonate reservoir stimulated with gelled acid. During production tests all wells showed excellent production results and reservoir flowing coverage confirmed by spectrum noise logs (SNL), high precision temperature (HPT) and production logs (PLT). Based on three wells results; it is concluded that openhole completion can offer a valuable completion option for well recovery & may be used for optimization for current designs. The cost of the barefoot completion delivery has reduced by 20%. The production output from the wells is higher than expected; Productivity Index of those wells is relatively much better than the nearby wells.\n The Newly proposed design provide continuity to develope Ara Salt wells and recovery plan to overcome challenges and avoiding well abandonments. This completion option was reviewed and accepted as base case completion for some deep fields in South of Oman, where oil is encapsulated in high-pressure carbonate floaters and there no risk of water or gas breakthrough. One more additional well was planned to be completed as openhole \"Barefoot\" completion and cost saving of ~15% over the total well cost was achieved. This recovery option will benefit all the upcoming future wells in the area.","PeriodicalId":11061,"journal":{"name":"Day 1 Mon, November 11, 2019","volume":"2 1","pages":""},"PeriodicalIF":0.0000,"publicationDate":"2019-11-11","publicationTypes":"Journal Article","fieldsOfStudy":null,"isOpenAccess":false,"openAccessPdf":"","citationCount":"0","resultStr":null,"platform":"Semanticscholar","paperid":null,"PeriodicalName":"Day 1 Mon, November 11, 2019","FirstCategoryId":"1085","ListUrlMain":"https://doi.org/10.2118/197356-ms","RegionNum":0,"RegionCategory":null,"ArticlePicture":[],"TitleCN":null,"AbstractTextCN":null,"PMCID":null,"EPubDate":"","PubModel":"","JCR":"","JCRName":"","Score":null,"Total":0}
引用次数: 0

Abstract

Well delivery in Pre-Cambrian salt with high-pressure floaters in the South of Oman provides several challenges, including Well Control Events, losses, supercharging, salt creeping, casing collapse and a negative drilling windows if section TD is picked incorrectly. The well design does not allow for an additional casing string with redundancy to case of troublesome zones. To overcome this, PDO initiated a barefoot completion as an extra hole section instead of well abandonment. As a wells recovery plan in 2017, PDO initiated different potential options to complete Ara salt wells and one of visible alternative options was to complete wells as open hole "Barefoot" completion. A design solution developed across technical functions on the suitability of barefoot completion in the carbonate reservoirs. The method to drill and complete with 3.615" hole as "Barefoot" was then expedited through detailed design as per the well delivery process. Key factors, which were considered included inflow performance and hole stability, the review of BHA design, drilling hydraulics, fluids selection and barrier considerations for barefoot completion. The operational challenges were reviewed and optimized with each implementation to drive further value. To date three wells recovered successfully with the new barefoot completion method. The wells completed with solids free drilling mud placed across the reservoir section and a suspension plug installed in the upper completion to facilitate rig release. During well testing operations; the suspension plug is removed, the openhole section is clean-up with coil tubing to remove filter cake with Enzyme treatment and finally the carbonate reservoir stimulated with gelled acid. During production tests all wells showed excellent production results and reservoir flowing coverage confirmed by spectrum noise logs (SNL), high precision temperature (HPT) and production logs (PLT). Based on three wells results; it is concluded that openhole completion can offer a valuable completion option for well recovery & may be used for optimization for current designs. The cost of the barefoot completion delivery has reduced by 20%. The production output from the wells is higher than expected; Productivity Index of those wells is relatively much better than the nearby wells. The Newly proposed design provide continuity to develope Ara Salt wells and recovery plan to overcome challenges and avoiding well abandonments. This completion option was reviewed and accepted as base case completion for some deep fields in South of Oman, where oil is encapsulated in high-pressure carbonate floaters and there no risk of water or gas breakthrough. One more additional well was planned to be completed as openhole "Barefoot" completion and cost saving of ~15% over the total well cost was achieved. This recovery option will benefit all the upcoming future wells in the area.
查看原文
分享 分享
微信好友 朋友圈 QQ好友 复制链接
本刊更多论文
裸眼完井作为穿越盐井和高压浮子钻井的采收率案例
在阿曼南部的前寒武纪盐层,使用高压浮子进行完井作业带来了一些挑战,包括井控事件、漏失、增压、盐蠕变、套管塌陷以及如果分段TD选择错误会导致钻井窗口的减少。该井的设计不允许额外的套管柱进行冗余,以防止出现问题。为了克服这个问题,PDO开始了赤脚完井,作为额外的井段,而不是弃井。作为2017年的油井恢复计划,PDO提出了不同的完井方案,其中一个明显的替代方案是裸眼“赤脚”完井。针对碳酸盐岩储层赤脚完井的适用性,开发了一种跨技术功能的设计方案。然后,根据交付过程,通过详细设计,加快了以“赤脚”方式钻完3.615英寸井眼的方法。考虑的关键因素包括流入性能和井眼稳定性、BHA设计评估、钻井水力学、流体选择和赤脚完井的屏障考虑。每次实施时,都会对操作挑战进行审查和优化,以推动进一步的价值。迄今为止,采用新的赤脚完井方法成功回收了3口井。完井时,在整个油藏段放置无固相钻井液,并在上部完井处安装悬浮塞,以方便钻机释放。在试井作业期间;移除悬浮塞,用盘管清理裸眼段,用酶处理去除滤饼,最后用凝胶酸对碳酸盐岩储层进行压裂。在生产测试过程中,所有井均显示出良好的生产效果,并通过频谱噪声测井(SNL)、高精度温度测井(HPT)和生产测井(PLT)证实了储层流动覆盖范围。根据三口井的结果;由此得出结论,裸眼完井可以为油井采收率提供一种有价值的完井选择,并可用于当前设计的优化。赤脚完井的成本降低了20%。这些井的产量高于预期;这些井的产能指数相对好于附近的井。新提出的设计为Ara盐井的开发和采收率计划提供了连续性,以克服挑战并避免弃井。该完井方案在阿曼南部的一些深层油田进行了评估,并被接受为基本完井方案,在这些油田中,石油被封装在高压碳酸盐浮子中,没有水或气突破的风险。计划再完成一口裸眼“赤脚”完井,比总成本节省约15%的成本。这种回收方案将使该地区未来所有的井受益。
本文章由计算机程序翻译,如有差异,请以英文原文为准。
求助全文
约1分钟内获得全文 去求助
来源期刊
自引率
0.00%
发文量
0
期刊最新文献
Lessons Learned from History-Matching the First Out-Of-Sequence Fracturing Field Test in North America Energy Saving Challenges and Opportunities in Upstream Operations using Value Methodology An Integrated Solution to Repair Multiple Shallow Leaks in Production Tubing – A Unique Single Trip Well Intervention Technique Openhole Completions as Recovery Case for Drilling Across Salt and High Pressure Floaters The Impact of Dynamic Filtration on Formation Testing in Low Mobility Carbonate Formations. Case Study: Lower Cretaceous Carbonate Reservoir in the UAE
×
引用
GB/T 7714-2015
复制
MLA
复制
APA
复制
导出至
BibTeX EndNote RefMan NoteFirst NoteExpress
×
×
提示
您的信息不完整,为了账户安全,请先补充。
现在去补充
×
提示
您因"违规操作"
具体请查看互助需知
我知道了
×
提示
现在去查看 取消
×
提示
确定
0
微信
客服QQ
Book学术公众号 扫码关注我们
反馈
×
意见反馈
请填写您的意见或建议
请填写您的手机或邮箱
已复制链接
已复制链接
快去分享给好友吧!
我知道了
×
扫码分享
扫码分享
Book学术官方微信
Book学术文献互助
Book学术文献互助群
群 号:481959085
Book学术
文献互助 智能选刊 最新文献 互助须知 联系我们:info@booksci.cn
Book学术提供免费学术资源搜索服务,方便国内外学者检索中英文文献。致力于提供最便捷和优质的服务体验。
Copyright © 2023 Book学术 All rights reserved.
ghs 京公网安备 11010802042870号 京ICP备2023020795号-1