Industry's First Sidetrack in 12-1/4-in Casing Enables Operator to Re-Establish Production in GOM

Tom Emelander
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Abstract

In a Gulf of Mexico (GOM) ultradeepwater well, liner integrity issues forced an operator to consider milling a conventional casing exit to sidetrack as deep as possible to re-establish production. Milling a window in 12 -1/4-in. heavy wall casing above the liner hanger had never been achieved before because of the thickness and grade of casing. A successful installation would require significant preplanning and testing to prove capability before real-world application. The service provider recommended an off-the-shelf solution to accommodate a 12 -1/4-in. casing exit. It was determined that the best fit for the application would be the standard equipment used for exits out of 10 -3/4-in. casing, given the similar internal diameters (IDs). Despite never having performed an installation in this casing size, the provider had a successful run history for exits in heavy weight casing strings. Job challenges included avoiding cutting a casing connection, managing swarf, milling through a centralizer, and achieving a low dogleg for production packers. Additional challenges included torque limitations, mill gauge, and the limestone formation. An 8-in. outside diameter (OD) system with mechanical anchor and 9 -7/8-in. OD mills was sent to a test well designed to replicate the target section of the offshore well. Based on determinations made in the planning phase, milling of the window and rathole would be staged in two trips. Additionally, a replica drilling bottom hole assembly (BHA), 8 -5/8-in. casing, and a replica production packer would need to pass through the window to ensure both window quality and low enough dogleg. Dogleg data was acquired through multiple logging runs during the 10-day operation. The installation went as planned, along with an additional custom window elongation run to decrease the dogleg severity to approximately 4.5°/100 -ft (30m). Having successfully validated the equipment for the application, the operator and servicer prover were comfortable moving onto the GOM well. Considering the test results, the team planned to mill the window and rathole in one trip. They achieved the 22 -ft long window and 15 -ft rathole in one run that lasted 26 hours. This installation is the first sidetrack conducted with a whipstock in 12 -1/4-in. casing. This paper shows that a safe, reliable casing exit installation is possible in difficult applications, such as uniquely heavy wall casing, even though it may previously have been considered impossible. This successful application provides the industry with contingency options in similar scenarios.
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业内首个12-1/4-in套管侧钻,帮助作业者在墨西哥湾恢复生产
在墨西哥湾(GOM)的一口超深水井中,尾管完整性问题迫使作业者考虑将常规套管出口磨铣至尽可能深的侧钻,以恢复生产。铣一个12 -1/4英寸的窗户。由于套管的厚度和等级,以前从未实现过尾管悬挂器上方的厚壁套管。成功的安装需要大量的预先计划和测试,以便在实际应用之前证明其能力。服务提供商推荐了一种现成的解决方案,以适应12 -1/4-in。肠衣出口。最终确定,最适合该应用的是用于10 -3/4-in出口的标准设备。考虑到相似的内径(id),尽管从未在这种套管尺寸下进行过安装,但该公司在重型套管的出口作业中取得了成功。作业挑战包括避免切割套管连接件、管理切屑、磨铣扶正器以及实现生产封隔器的低狗腿。其他挑战包括扭矩限制、磨尺和石灰岩地层。一个8。外径(OD)系统具有机械锚和9 -7/8-in。将OD磨粒送入测试井,以复制海上井的目标段。根据规划阶段的决定,磨铣窗口和鼠眼将在两次下钻中完成。此外,还有一个8- 5/ 8in的复制钻具底部钻具组合(BHA)。套管和复制生产封隔器需要穿过窗口,以确保窗口质量和足够低的狗腿。在10天的作业中,通过多次测井获得了狗腿数据。安装按计划进行,同时还增加了一个定制窗口延伸,将狗腿的严重程度降低到大约4.5°/100英尺(30米)。在成功验证了设备的应用后,作业者和服务证明人员可以轻松地进入墨西哥湾井。考虑到测试结果,该团队计划在一次作业中磨平窗口和鼠孔。他们在一次作业中完成了22英尺长的窗户和15英尺长的鼠洞,历时26小时。该装置是第一次使用12 -1/4-in斜向器进行侧钻。套管。本文表明,在一些困难的应用中,例如特殊的厚壁套管,安全可靠的套管出口安装是可能的,尽管这在以前可能被认为是不可能的。这个成功的应用程序为行业在类似场景中提供了应急选择。
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