Using Advance Acid Fracturing Design to Increase the Production Efficiency in a HPHT Reservoir: A Success Story from Southern Mexico

F. Figueroa, Gustavo Mejías, J. Frias, Bonifacio Brito, Diana L. Velázquez, Carmen J. Ramírez, F. Téllez, Juan Briceño, J. Salas, Ángel Olivares, Georgina Olán, Andrés Flores, Jesús Arroyo, John E. Busteed, René Hernández, J. Gonzalez
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Abstract

Enhanced hydrocarbon production in a high-pressure/high-temperature (HP/HT) carbonate reservoir, involves generating highly conductive channels using efficient diversion techniques and custom-designed acid-based fluid systems. Advanced stimulation design includes injection of different reactive fluids, which involves challenges associated with controlling fluid leak-off, implementing optimal diversion techniques, controlling acid reaction rates to withstand high-temperature conditions, and designing appropriate pumping schedules to increase well productivity and sustainability of its production through efficient acid etching and uniform fluid distribution in the pay zone. Laboratory tests such as rock mineralogy, acid etching on core samples and solubility tests on formation cuttings were performed to confirm rock dissolving capability, and to identify stimulation fluids that could generate optimal fracture lengths and maximus etching in the zone of interest while corrosion test was run to ensure corrosion control at HT conditions. After analyzing laboratory tests results, acid fluid systems were selected together with a self-crosslinking acid system for its diversion properties. In addition, customized pumping schedule was constructed using acid fracturing and diverting simulators and based on optimal conductivity/productivity results fluid stages number and sequence, flow rates and acid volumes were selected. The engineered acid treatment generated a network of conductive fractures that resulted in a significant improvement over initial production rate. Diverting agent efficiency was observed during pumping treatment by a 1,300 psi increase in surface pressures when the diverting agent entered the formation. Oil production increased from 648.7 to 3105.89 BPD, and gas production increased from 4.9 to 26.92 MMSCFD. This success results demonstrates that engineering design coupled with laboratory tailor fluids designs, integrated with a flawless execution, are the key to a successful stimulation. This paper describes the details of acidizing technique, treatment design and lessons learned during execution and results.
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采用先进的酸压裂设计提高高温高压油藏的生产效率:墨西哥南部的成功案例
在高压/高温(HP/HT)碳酸盐岩储层中,提高油气产量需要使用高效的导流技术和定制的酸基流体体系来形成高导流通道。先进的增产设计包括注入不同的反应性流体,其中包括控制流体泄漏、实施最佳导流技术、控制酸反应速率以承受高温条件,以及设计适当的泵送计划,通过有效的酸蚀和均匀的产层流体分布来提高油井产能和可持续性生产。通过岩石矿物学、岩心样品的酸蚀和地层岩屑的溶解度等实验室测试来确认岩石溶解能力,并确定能够在目标区域产生最佳裂缝长度和最大腐蚀的增产液,同时进行腐蚀测试以确保高温条件下的腐蚀控制。在分析了实验室测试结果后,选择了酸液体系和自交联酸体系,以考察其导流性能。此外,利用酸压裂和分流模拟器构建了定制的泵送计划,并根据最佳导流能力/产能结果选择了流体级数和顺序、流速和酸体积。工程酸化处理产生了一个导电性裂缝网络,显著提高了初始产量。在泵送处理过程中,当暂堵剂进入地层时,地面压力增加了1300 psi,从而观察到暂堵剂的效率。石油产量从648.7桶/天增加到3105.89桶/天,天然气产量从4.9百万立方英尺/天增加到26.92万立方英尺/天。这一成功的结果表明,工程设计与实验室定制流体设计相结合,再加上完美的执行,是成功增产的关键。本文详细介绍了酸化技术、处理设计、实施过程中的经验教训和效果。
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