Reduction of Sulfur Species in LNG to Ultra Low Levels

N. Ali, Haitham Abdulla, Ahmed Al Ameeri, M. Jacques, Ilhem Kouaiche
{"title":"Reduction of Sulfur Species in LNG to Ultra Low Levels","authors":"N. Ali, Haitham Abdulla, Ahmed Al Ameeri, M. Jacques, Ilhem Kouaiche","doi":"10.2118/192626-MS","DOIUrl":null,"url":null,"abstract":"\n ADNOC LNG and TechnipFMC are reviewing options to reduce total sulphur in LNG, from a current realized specification of 4-9 mgS/Nm3, down to less than 1 mgS/Nm3. The requirement is to enhance the quality of the LNG product, and reduce environmental emissions.\n Several technologies were reviewed, including options to hydrolyze COS present in wet sweet gas, introduction of desulphurization beds downstream the dehydration units, and changing the type of molecular sieves. Those options were extensively reviewed, and found to be inadequate on their own. Therefore, solvent swap within the Acid Gas Removal Unit (AGRU) along with Molecular sieve upgrade was found to be the most viable option.\n Rigorous efforts were put in place to establish a robust roadmap that serves furnishing the correct basis, defining the required assessments and developing the intended approach and tools.\n This paper aims to present the overall methodology, approach and efforts undertaken to study the means to reduce sulphur species in LNG, in the present three LNG trains.","PeriodicalId":11208,"journal":{"name":"Day 2 Tue, November 13, 2018","volume":"31 1","pages":""},"PeriodicalIF":0.0000,"publicationDate":"2018-11-12","publicationTypes":"Journal Article","fieldsOfStudy":null,"isOpenAccess":false,"openAccessPdf":"","citationCount":"0","resultStr":null,"platform":"Semanticscholar","paperid":null,"PeriodicalName":"Day 2 Tue, November 13, 2018","FirstCategoryId":"1085","ListUrlMain":"https://doi.org/10.2118/192626-MS","RegionNum":0,"RegionCategory":null,"ArticlePicture":[],"TitleCN":null,"AbstractTextCN":null,"PMCID":null,"EPubDate":"","PubModel":"","JCR":"","JCRName":"","Score":null,"Total":0}
引用次数: 0

Abstract

ADNOC LNG and TechnipFMC are reviewing options to reduce total sulphur in LNG, from a current realized specification of 4-9 mgS/Nm3, down to less than 1 mgS/Nm3. The requirement is to enhance the quality of the LNG product, and reduce environmental emissions. Several technologies were reviewed, including options to hydrolyze COS present in wet sweet gas, introduction of desulphurization beds downstream the dehydration units, and changing the type of molecular sieves. Those options were extensively reviewed, and found to be inadequate on their own. Therefore, solvent swap within the Acid Gas Removal Unit (AGRU) along with Molecular sieve upgrade was found to be the most viable option. Rigorous efforts were put in place to establish a robust roadmap that serves furnishing the correct basis, defining the required assessments and developing the intended approach and tools. This paper aims to present the overall methodology, approach and efforts undertaken to study the means to reduce sulphur species in LNG, in the present three LNG trains.
查看原文
分享 分享
微信好友 朋友圈 QQ好友 复制链接
本刊更多论文
将液化天然气中的硫化物降至超低水平
ADNOC LNG和TechnipFMC正在审查减少液化天然气总硫的方案,从目前实现的4-9 mg /Nm3的规格降至低于1 mg /Nm3。要求是提高液化天然气产品的质量,减少环境排放。综述了几种技术,包括水解湿式甜气中COS的选择、在脱水装置下游引入脱硫床以及改变分子筛的类型。对这些备选办法进行了广泛审查,发现它们本身是不够的。因此,在酸性气体去除装置(agu)内进行溶剂交换以及分子筛升级是最可行的选择。严格的工作已经到位,以建立一个健壮的路线图,提供正确的基础,定义所需的评估,并开发预期的方法和工具。本文旨在介绍在目前的三列液化天然气列车中研究减少液化天然气中硫种的总体方法、方法和努力。
本文章由计算机程序翻译,如有差异,请以英文原文为准。
求助全文
约1分钟内获得全文 去求助
来源期刊
自引率
0.00%
发文量
0
期刊最新文献
Crisis as Source of Innovation Strategy at ADNOC LNG Successful Implementation of Torque and Drag Management Techniques in High Departure Wells is the Key to Safely Reach Wells Planned Total Depth in Offshore Artificial Islands Efficiency, Economics and Compliance: A Practical Planning Tool for Optimizing Cuttings Treatment First Cross-Dipole Shear Wave Imaging Application for Intersecting a Mother Open-Hole from a Near-Parallel Side-Track Wellbore Effect of Drilling Muds Wall Slip on Reliable Frictional Pressure Loss Estimations in Offshore Drilling
×
引用
GB/T 7714-2015
复制
MLA
复制
APA
复制
导出至
BibTeX EndNote RefMan NoteFirst NoteExpress
×
×
提示
您的信息不完整,为了账户安全,请先补充。
现在去补充
×
提示
您因"违规操作"
具体请查看互助需知
我知道了
×
提示
现在去查看 取消
×
提示
确定
0
微信
客服QQ
Book学术公众号 扫码关注我们
反馈
×
意见反馈
请填写您的意见或建议
请填写您的手机或邮箱
已复制链接
已复制链接
快去分享给好友吧!
我知道了
×
扫码分享
扫码分享
Book学术官方微信
Book学术文献互助
Book学术文献互助群
群 号:481959085
Book学术
文献互助 智能选刊 最新文献 互助须知 联系我们:info@booksci.cn
Book学术提供免费学术资源搜索服务,方便国内外学者检索中英文文献。致力于提供最便捷和优质的服务体验。
Copyright © 2023 Book学术 All rights reserved.
ghs 京公网安备 11010802042870号 京ICP备2023020795号-1