Water-Flood Management in a Mature Field Through Pilot Approach

A. Thapliyal, Sudeb Kundu, Suparna Chowdhury, Harjinder Singh
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Abstract

A successful water injection management is a key to increase or stabilize oil production and to maximize oil recovery from a mature field. This paper describes an approach to draw maximum benefit through existing set up of a water injection in a mature offshore carbonate field of India. Water injection initiated after the six years of oil production and field is under water flood since last 28 years. The field witnessed favorable water flood condition and almost negligible aquifer support. During its long production period most of the producers had been sideracked from one to three times to target better saturation areas which has led to uneven subsurface water distribution. The field has also suffered less voidage compensation for quite some time. To understand and mitigate the problem, a small pilot area within a field has been selected for implementing a good surveillance and monitoring program with pattern injection and possible intervention strategy. It was decided that based on the success of this pilot, the concept would be developed for implementation in step by step manner for entire field. The importance of multidisciplinary team has been recognized and detailed SWOT analysis was done for effective implementation of plan. Initially pilot area comprised of 15 oil producers and 4 water injectors. Conversion of one producer to water injector and restoration of water injection in 3 injectors were done as per plan and optimized injection rate (in this case maximum 3000 bbl per day) per injector were implemented. Peripheral pattern for pilot area with 5 injectors and 5 spot inverted patterns from rest 3 injectors were decided. After one year of the implementation a thorough performance analysis of the pilot has been carried out which indicates the overall improvement of liquid and oil production rates along with reduction in GOR and decreasing trend of oil decline rates of producers. The pilot approach has certainly helped to understand the Reservoir conformance in short duration of time. Encouraging results of this methodology guides to extent and implement this approach in other parts of field to cover the entire field in phased manner.
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成熟油田注水管理试点研究
成功的注水管理是提高或稳定石油产量、最大限度地提高成熟油田采收率的关键。本文介绍了一种利用印度海上成熟碳酸盐岩油田现有注水装置获得最大效益的方法。该油田开采6年后开始注水,28年来一直处于水驱状态。油田注水条件良好,含水层支撑几乎可以忽略不计。在漫长的生产过程中,为了寻找较好的饱和区域,大部分生产井都进行了1 ~ 3次侧推,导致地下水分布不均匀。在相当长的一段时间里,该领域也遭受了较少的损失补偿。为了了解和缓解问题,在油田内选择了一个小的试点区域,实施良好的监测和监测计划,包括模式注入和可能的干预策略。会议决定,在这一试点成功的基础上,将发展这一概念,以便在整个地区逐步实施。认识到多学科团队的重要性,并对计划的有效实施进行了详细的SWOT分析。最初的试验区包括15个采油厂和4个注水井。按照计划,将一个采油器转换为注水井,并恢复了3个注水井的注水井,并优化了每个注水井的注入速度(在这种情况下,最大注入量为3000桶/天)。确定了试验区5个喷射器的周边模式和其余3个喷射器的5个点倒转模式。在实施一年后,对试点进行了全面的绩效分析,结果表明,随着GOR的降低,生产商的出油率呈下降趋势,液产率和产油量都得到了全面改善。试点方法无疑有助于在短时间内了解储层的特征。这一方法的令人鼓舞的结果指导了在该领域的其他部分扩大和实施这一方法,以分阶段的方式覆盖整个领域。
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