高炉工艺用铁矿石烧结机的研制

Femi Akinfolarin, B. Kareem, Oladunni Oyetola Alabi
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引用次数: 0

摘要

铁精矿在进入高炉进一步加工前,必须有适当的烧结、结块手段。使用本地采购的低碳钢材料设计和制造了一台容量为5公斤的烧结矿机。该机器采用30 × 30 cm,深15cm的燃烧室制造。它还内衬耐火材料,以减少室的体积为3375 cm3。然而,烧结室被设计成一个截断的方形金字塔形状,在内衬耐火材料后,体积为2150 cm3。本设计以焦炭和棕榈仁壳炭为燃料,将其点燃后,通过将热量吸进烧结结块的矿石中,向烧结材料中产生热量。按照ASTM E276和E389标准对烧结产品进行了滚转指数、磨损、孔隙率等试验。试验结果表明,焦炭和棕榈仁壳的翻滚指数分别为70.2%和65.7%。焦炭和棕榈仁炭的磨损指数分别为5.1%和4.6%,孔隙率分别为6.8%和6.5%。实验测试的结果与其他研究工作是一致的。因此,所研制的铁矿石烧结机生产高炉运行用烧结矿的效率较高。
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Development of iron ores sintering machine for blast furnace process
There must be proper means to sinter and, agglomerated iron ore concentrate before it can be further processed in the blast furnace. A Sintering machine of 5kg capacity of agglomerated ore was designed and fabricated using mild steel material, which was locally sourced. The machine was fabricated with a combustion chamber of 30 by 30 cm and with 15cm depth. It was also lined with refractory material to reduce the chamber to the volume of 3375 cm3. However, the sintering chamber was designed to have a truncated square pyramid shape to the volume of 2150 cm3 after lining with refractory material. The design was made to utilize coke and palm kernel shell char as fuel which will be ignited to produce heat into the sintered material by suction of the heat into the agglomerated sintered ore. Tests such as tumbler index, abrasion, and porosity test were carried out on the sintered products in agreement with ASTM E276 and E389 standards. The results from the test gave a tumbler index of 70.2% and 65.7% for coke and palm kernel shells respectively. Also, abrasion index of 5.1% and 4.6% for coke and palm kernel char, and porosity of 6.8% and 6.5% for coke and palm kernel char respectively. The results from the experimental test were in agreement with other research work. Therefore, the developed iron ore sintering machine has a better efficiency of producing sinter for blast furnace operation.   
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