手工装配线的精益生产-案例研究

Low Shye Nee, Goh Wen Juin, Fow Jun Yan, C. Y. Theng, S. Kamaruddin
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引用次数: 7

摘要

本文描述了在一家电子通信塑料零部件供应商中进行的改进项目的方法。本文的重点是运用精益工具对人工装配线进行工艺改进,采用精益工具对人工装配线进行工艺改进。过程改进分为几个阶段,从定义目标到解决方案的测试运行,不同的阶段使用不同的精益概念。改进是分阶段进行的,以确保改进的效果。通过试运行,提出的基于精益生产理念的解决方案提高了运行中空转时间减少(81.64%)和操作员节省(40%)的盈利能力。
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Lean production in manual assembly line — A case study
This paper is describing a methodology of improvement project that is carried out in a company that supplies electronic communication plastic parts. By using the lean tools, the focus of the paper is to improve the manual assembly line by adopting lean tool for the process improvement. The process improvement are divided into several phases, from defining the goal until the test run of the solution, with different lean concept being used at different phase. The improvement had been done phase by phase in order to ensure the impact of the improvement. Through the test run, the proposed solution based on concept of Lean production increase profitability based on idling time reduction (81.64%) and operator saving(40%) in operation.
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