俄罗斯国家石油公司在Odoptu-More油田成功交付了最长的油井

A. Shakhova, I. Lebedeva, Oleg Valshin, Robert Famiev, D. Marushkin, Roman Savinov, A. Dementyev, A. Shatilov, A. Khakov, A. Shakirova, D. Gaskov, V. Bochkarev, Vladimir Surmin
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摘要

本文介绍了在库页岛Odoptu-more油田(North Dome)应用综合方法钻出最长大位移井的结果。尽管运营商在Odoptu-more油田已经钻了许多大位移钻井(ERD)井,但大位移井总是需要新的解决方案。由于Odoptu-more油田的8 - 1 / 2 in生产段的立管压力(SPP)和当量循环密度(ECD)很高,采用标准井设计无法到达偏远油藏。工程研究结果表明,一口井的设计尺寸部分增大,将9 - 5/8-in套管改为尾管,随后面临的挑战是:由于管柱屈曲,9 - 5/8-in尾管无法下至要求的深度。在该项目中实施了几项关键技术解决方案,从而实现了最长井的无事故生产。这些解决方案包括修改井设计,允许钻8- 1 / 2英寸的生产段以到达偏远的油藏,并在该项目中首次使用“泥浆悬浮”浮选技术将9 - 5/8英寸的尾管输送到所需的深度。采用综合方法后,项目组在Odoptu-more油田以总测量深度8699m、ERD比4.89、定向难度指数(DDI) 7.6的成绩打破了最长井的新纪录(Alistair W. Oag 2000)。钻大位移ERD井为作业者提供了机会,可以在不改变现有平台设施的情况下,到达离陆地钻井平台更远的海上含油油藏并投入生产。
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Integrated Approach Enabled Successful Delivery of the Longest Well on Odoptu-More Field for Russian National Oil Company
This paper provides the results of the application of integrated approach to drill the longest extended reach well which has ever been drilled in Odoptu-more field (North Dome) in Sakhalin. Although many extended reach drilling (ERD) wells have been already drilled by the operator in Odoptu-more field, extreme reach wells always require new solutions. Reaching remote reservoirs by applying standard well design of Odoptu-more field was not possible due to high standpipe pressure (SPP) and equivalent circulating density (ECD) in 8 ½-in production section. Engineering study resulted in partial upsize of a well design and change 9 5/8-in casing to liner followed by remaining challenges: 9 5/8-in liner could not be delivered to required depth due to string buckling. Several key technical solutions were implemented in the project thus allowing to deliver the longest well accident-free. Those solutions included well design modification allowing to drill 8 ½-in production section to reach remote reservoirs and 9 5/8-in liner delivery to the required depth using "mud over air" flotation technique for the first time in the project. Having applied integrated approach, the project team broke a new record in drilling the longest well at Odoptu-more field with total measured depth 8699m, ERD ratio 4.89 and Directional Difficulty Index (DDI) of 7.6 (Alistair W. Oag 2000). Drilling extreme reach ERD well unlocked opportunities for the operator to reach and put into the production more distant offshore oil-bearing reservoirs from the land rig without changing existing pad facilities.
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