纵缝焊接高温封头失效研究

J. F. Henry, F. Ellis, J. Alice, J. LaFontaine, P. Orban
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引用次数: 0

摘要

PENELEC公司的Shawville 3号机组在板形封头中检测到泄漏,因此开始了广泛的故障调查,以确定纵向焊缝可见裂缝的起源。由SA387-D材料制成,设计用于过热器出口温度为566摄氏度,11.4厘米厚的集箱在故障发生时已经运行了大约187,000小时。讨论的重点是对从故障附近的纵缝焊件和箱头的其他区域取出的船样进行金相检查的结果,这些区域被认为已经达到了峰值温度。通过蠕变试验测定了服役暴露母材和蠕变损伤焊缝金属的长期力学性能。根据公用事业公司在一到三年内更换集管的决定,采用了等应力过温铅样品方法,即实验室测试样品的失败将先于工厂的失败。这些测试显示,与焊接金属相比,母材的寿命相差约2:1。
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Failure Investigation of Longitudinal Seam Welded Elevated Temperature Header
As the result of a leak detected in a plate-formed header at PENELEC'S Shawville Unit No. 3, an extensive failure investigation was initiated to determine the origin of cracking visible along the longitudinal weld seam. Fabricated from SA387-D material and designed for a superheater outlet temperature of 566 deg C, the 11.4 cm thick header had operated for approximately 187,000 h at the time of the failure. Discussion focuses on the results of a metallographic examination of boat samples removed from the longitudinal seam weldment in the vicinity of the failure and at other areas of the header where peak temperatures were believed to have been reached. The long-term mechanical properties of the service-exposed base metal and creep-damaged weld metal were determined by creep testing. Based on the utility's decision to replace the header within one to three years, an isostress overtemperature lead specimen approach was taken, whereby failure of a test specimen in the laboratory would precede failures in the plant. These tests revealed approximately a 2:1 difference in life for the base metal as compared to weld metal.
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