通过非钻机部署的有线技术恢复生产

W. J. Diwaku, H. Sambo, J. M. Sonhi, A. A. Saadi, M. Wallach
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摘要

目标/范围:本文详细介绍了地层隔离阀 (FIV) 故障后恢复生产所面临的挑战和采用的解决方案。方法、程序、过程:在部署上部完井期间,安装了 FIV 以隔离储层。井口、井树和流线连接好后,多次尝试打开阀门以启动生产。尽管按计划进行了压力循环,但 FIV 没有打开。人们怀疑是阀门顶部的填充物/碎片阻碍了阀门的液压启动。FIV 的失灵以及相关的生产损失促使团队制定了一项补救干预计划。操作员和业务合作伙伴团队评估了多种替代方案,最终选择了一种结合滑触线和电力线拖拉机部署的解决方案。该计划包括一次漂移作业,以确定 FIV 上方的井筒状况,随后进行一次清理作业,并铣削 FIV 的铬镍铁合金球阀。由于井眼角度较大,需要使用拖拉机对铣头施加压力。结果、观察结果和结论:在使用光滑管线救助器和电动管线(EL)抽吸工具清除井筒碎片后,部署了拖拉机铣削组件,成功铣削了 FIV 球阀。成功的铣削作业使油井恢复到钻井前估计的生产水平,节省了约 3000 万美元的主要钻机工作超额成本。新颖/补充信息:本文介绍了设计最佳干预计划的过程,以及详细的规划和操作步骤。最佳工程解决方案与执行过程中的操作规范相结合,成功地使油井恢复生产,最大限度地降低了生产成本损失,同时避免了昂贵的钻机干预。本文还重点介绍了所采用的新技术、铣削 BHA 配置、具体的经验教训以及执行过程中记录的最佳实践。
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Restoring Production Via Non-Rig Deployed Wireline Technology
Objectives/Scope: This paper details the challenges faced and the solutions deployed to restore production following failure of a formation isolation valve (FIV). Methods, Procedures, Process: The FIV was installed to isolate the reservoir during the deployment of the Upper Completion. Once the wellhead, tree, and flowlines were hooked up, several attempts were made to open the valve to initiate production. Despite the planned pressure cycles being applied, the FIV did not open. It was suspected that there was fill/debris on top of the valve preventing its hydraulic activation. The failure of the FIV, and associated lost production, drove the team to develop a remedial intervention plan. The Operator and Business Partner team evaluated multiple alternatives before selecting a combined slickline and electric line tractor-deployed solution. The plan included a drift run to determine the wellbore condition above the FIV, followed by a cleanout run and the milling of the FIV Inconel ball-valve. Due to the high hole angle, a tractor was required to apply weight on the mill bit. Results, Observations, Conclusions: After the removal of the wellbore debris using a slickline bailer and a suction tool deployed with electric line (EL), a tractor milling assembly was deployed that successfully milled through the FIV ball-valve. The successful milling operation saved approximately $30MM in Major Rig Work Over cost by bringing the well back to production levels in accordance with the pre-drill estimates. Novel/Additive Information: This paper describes the process followed to design an optimal intervention plan, and the detailed planning and operational steps. The optimal engineered solution coupled with operational discipline during execution successfully brought the well back to production, minimizing the lost production cost while avoiding a costly rig-based intervention. This paper also highlights the novel technologies utilized, the milling BHA configuration, specific lessons learned, and best practices recorded during the execution.
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