{"title":"某140mw火电厂二次过热加热器管失效分析","authors":"Atanu Saha, H. Roy","doi":"10.1016/j.csefa.2017.05.001","DOIUrl":null,"url":null,"abstract":"<div><p>This article describes the findings of a detailed investigation into the failure of a secondary super heater tube in a 140<!--> <!-->MW thermal power plant. Preliminary macroscopic examinations along with visual examination, dimensional measurement and chemical analysis were carried out to deduce the probable cause of failure. In addition optical microscopy was a necessary supplement to understand the cause of failure. It was concluded that the tube had failed due to severe creep damage caused by high metal temperature during service. The probable causes of high metal temperature may be in sufficient flow of steam due to partial blockage, presence of thick oxide scale on ID surface, high flue gas temperature etc. rupture.</p></div>","PeriodicalId":91224,"journal":{"name":"Case studies in engineering failure analysis","volume":"8 ","pages":"Pages 57-60"},"PeriodicalIF":0.0000,"publicationDate":"2017-04-01","publicationTypes":"Journal Article","fieldsOfStudy":null,"isOpenAccess":false,"openAccessPdf":"https://sci-hub-pdf.com/10.1016/j.csefa.2017.05.001","citationCount":"22","resultStr":"{\"title\":\"Failure investigation of a secondary super heater tube in a 140 MW thermal power plant\",\"authors\":\"Atanu Saha, H. Roy\",\"doi\":\"10.1016/j.csefa.2017.05.001\",\"DOIUrl\":null,\"url\":null,\"abstract\":\"<div><p>This article describes the findings of a detailed investigation into the failure of a secondary super heater tube in a 140<!--> <!-->MW thermal power plant. Preliminary macroscopic examinations along with visual examination, dimensional measurement and chemical analysis were carried out to deduce the probable cause of failure. In addition optical microscopy was a necessary supplement to understand the cause of failure. It was concluded that the tube had failed due to severe creep damage caused by high metal temperature during service. The probable causes of high metal temperature may be in sufficient flow of steam due to partial blockage, presence of thick oxide scale on ID surface, high flue gas temperature etc. rupture.</p></div>\",\"PeriodicalId\":91224,\"journal\":{\"name\":\"Case studies in engineering failure analysis\",\"volume\":\"8 \",\"pages\":\"Pages 57-60\"},\"PeriodicalIF\":0.0000,\"publicationDate\":\"2017-04-01\",\"publicationTypes\":\"Journal Article\",\"fieldsOfStudy\":null,\"isOpenAccess\":false,\"openAccessPdf\":\"https://sci-hub-pdf.com/10.1016/j.csefa.2017.05.001\",\"citationCount\":\"22\",\"resultStr\":null,\"platform\":\"Semanticscholar\",\"paperid\":null,\"PeriodicalName\":\"Case studies in engineering failure analysis\",\"FirstCategoryId\":\"1085\",\"ListUrlMain\":\"https://www.sciencedirect.com/science/article/pii/S221329021730038X\",\"RegionNum\":0,\"RegionCategory\":null,\"ArticlePicture\":[],\"TitleCN\":null,\"AbstractTextCN\":null,\"PMCID\":null,\"EPubDate\":\"\",\"PubModel\":\"\",\"JCR\":\"\",\"JCRName\":\"\",\"Score\":null,\"Total\":0}","platform":"Semanticscholar","paperid":null,"PeriodicalName":"Case studies in engineering failure analysis","FirstCategoryId":"1085","ListUrlMain":"https://www.sciencedirect.com/science/article/pii/S221329021730038X","RegionNum":0,"RegionCategory":null,"ArticlePicture":[],"TitleCN":null,"AbstractTextCN":null,"PMCID":null,"EPubDate":"","PubModel":"","JCR":"","JCRName":"","Score":null,"Total":0}
Failure investigation of a secondary super heater tube in a 140 MW thermal power plant
This article describes the findings of a detailed investigation into the failure of a secondary super heater tube in a 140 MW thermal power plant. Preliminary macroscopic examinations along with visual examination, dimensional measurement and chemical analysis were carried out to deduce the probable cause of failure. In addition optical microscopy was a necessary supplement to understand the cause of failure. It was concluded that the tube had failed due to severe creep damage caused by high metal temperature during service. The probable causes of high metal temperature may be in sufficient flow of steam due to partial blockage, presence of thick oxide scale on ID surface, high flue gas temperature etc. rupture.