中东某油井井喷事故原因分析及成功控制

Rahman Ashena, Farzad Ghorbani, Muhammad Mubashir, Mahdi Nazari Sarem, Amin Iravani
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引用次数: 2

摘要

2017年,中东地区的一口钻井发生井喷和爆炸。钻进至2610米深度后,决定起下钻更换钻头。当工作人员将钻柱拉出井眼时,钻柱深度为1332 m,发生井喷爆炸。该井为几乎水平(82度斜度)钻入油田高压气顶产油区的开发井。在本文中,在简要解释了事故的根本原因之后,我们介绍了为制止井喷而采用的井喷控制方法。同时采用顶压法和减压井底压法控制井喷。最后,58天后,井喷通过压底成功控制。在顶压作业期间,所有设备都被清理干净,这有助于在减压井成功后立即进行永久弃井。最后,定性地讨论了井喷对环境的不利影响(HSE)。
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The Root Cause Analysis and Successful Control of an Oilwell Blowout in the Middle East
In 2017, a blowout and explosion occurred in a drilling oilwell in the Middle East. After drilling to the depth of 2,610 m, tripping was decided in order to change the bit. When the crew were pulling the drill string out of the hole with the drill-string being at the depth of 1332 m, blowout and explosion occurred. The well was a development well drilling almost horizontally (82 degrees inclination angle) into a highly-pressured gas-cap and oil pay-zone of the oilfield. In this work, following a brief explanation of the root causal factors of the incident, we give an account of the blowout control methods applied to put an end to the blowout. Both the top-kill method and the bottom-kill method by relief well drilling, were simultaneously implemented to control the blowout. Finally, the blowout was successfully controlled by the bottom-kill after 58 days. During top-kill operations, all equipment was cleared away and this contributed to proceeding to permanent abandonment immediately after the relief well success. Finally, the adverse effect of the blowout on the environment (HSE) was qualitatively discussed.
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